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Gerhard Schiller
Gerhard Schiller
Gerhard Schiller
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G63 Accident
0:29
3 месяца назад
Laser Cleaning Rusty Tool
1:51
3 месяца назад
LASER PAINT STIPPING
0:51
3 месяца назад
Laser Cleaning on Turn Table
0:57
4 месяца назад
Laser Clean Weld Prep ASCO
1:01
4 месяца назад
Laser Cleaning Rust and Paint
1:25
4 месяца назад
Cl1
2:30
4 месяца назад
Robot Welding Angled Post 1
6:19
7 месяцев назад
December 3, 2023
1:07
8 месяцев назад
Telescopic Slide Gate Braswell Residence test
0:17
11 месяцев назад
20230730131015 006320r
0:30
Год назад
Custom Railing and Panel Production
6:17
3 года назад
Channel Pulse Weld
0:28
4 года назад
Panel Banding
2:47
4 года назад
Ironworker Press 45ton
2:12
5 лет назад
robotic welding panel production
1:28
5 лет назад
suspect
1:33
5 лет назад
20180922 122624
3:23
5 лет назад
Drill detail
0:39
10 лет назад
Multi spindle operation
1:21
10 лет назад
Multi spindle drill
0:56
10 лет назад
Комментарии
@DashcamNation1
@DashcamNation1 3 месяца назад
Hey Gerhard, may I feature your most recent video "G63 Accident" on my channel? Credited on screen & link in description. Any updates what happened afterwards?
@RRBDDrivingSchool
@RRBDDrivingSchool 3 месяца назад
where did it happen?
@RRBDDrivingSchool
@RRBDDrivingSchool 3 месяца назад
Hi Gerhard Schiller, can I use this video "G63 Accident" in my compilation of dashcam clips?with credit (name on screen).Any comment?update?
@vomitor90
@vomitor90 3 месяца назад
Hi, where did you bought that nozzle cleaner?
@matasvalentinavicius1288
@matasvalentinavicius1288 4 месяца назад
Well explained, your voice is well suited for the videos
@gerhard5911
@gerhard5911 4 месяца назад
Thx, been many years ago. I would do it different now I guess. Less of the hammering lol
@gerhard5911
@gerhard5911 7 месяцев назад
How did you built your enclosure? Door? Just wondering. The front door with glass on mine opens up like a lift gate with gas struts. You saw the slide up door. Just an air piston and cables. And the side with the equipment can opens like a lift gate by inwards. If you’d like I can take pics with more details.
@brad3378
@brad3378 7 месяцев назад
I saw one of your comments on the Ramsey Laser Press Brake channel (Video title: I imported a Fiber Laser Cutter From China) and I am glad I clicked on your name! Your system looks phenomenal and includes all of the same safety features that I would have designed into my own rig! I especially like your laser safety window which must have cost you $thousands. Thanks for sharing!
@gerhard5911
@gerhard5911 7 месяцев назад
Thanks for your compliments. Works pretty well. The windows did cost about $ 1,500 in materials in part because I made sure its the real thing with correct rating. When I started shopping for that I had some sticker shock.
@brad3378
@brad3378 7 месяцев назад
@@gerhard5911 Do you have any tips for safely verifying your safety glass is for the correct light spectrum? Will scratches make in unsafe? I am paranoid about laser safety.. When I build my system I am considering skipping the glass and using solid material with a few security cameras inside with a display on the outside
@gerhard5911
@gerhard5911 7 месяцев назад
Hi, also added 4 security cameras in addition to the window and added a large monitor. I am also paranoid about laser safety (eyesight). I can’t fathom all the open machines. May be in a one person shop. We have too many people moving through shop. And even then I looked by mistake without glasses. So here is what I did about the glass: 1. I ruled out any whatever acrylic plexi not specifically labeled for laser 2. I searched for wave length spectrum 900 to 1200 or similarand made sure it’s a level 8 density. 3. If it was too cheap I skipped. 4.checked sellers info feedback ect I can’t scientifically test but here is what I did. I tried to cut it with the laser. Expected it didn’t work no matter what I through at it. I got minor scoring. Like 0.2mm deep. And the sheet metal below was completely untouched. So I figured no laser energy passing through. Did the same with the blue acrylic panels. I also sealed off gaps in the enclosure so there is no straight path anywhere. Some of the open guy machines may be laughing. Right now there is so little real world data about accidents so I decided to play it safe. Never mind I have a professional shop and have an obligation (OSHA, insurance ect.) to make best efforts to provide safety from reasonably assumed dangers. With all the safety warnings everywhere there is. I way I could argue an open machine was reasonably safe standard if and accident would happen. It may be considered gross negligible (criminal) and I am not risking my eyesight either.
@gerhard5911
@gerhard5911 7 месяцев назад
And no, scratches don’t make it unsafe as it’s not a coating but solid dense to light
@brad3378
@brad3378 7 месяцев назад
@@gerhard5911 Thank you for such a great response! I am going to print this out to keep in my project build-binder.
@vxnova1
@vxnova1 9 месяцев назад
Punch out the wheel studs, you can use a longer bolt with a nut to pry out the bearing, On my case it split the bearing in 2 which allowed me to lay it on top of a couple of 4x4 boards and hammer out the bearing. It would be more stable than holding onto the assembly and beating on it, In my case the bearing was really seized and it took a considerable amount of beating to remove, Good video,
@ToxicTom1967
@ToxicTom1967 9 месяцев назад
very cool
@johncole3010
@johncole3010 2 года назад
You remind me of Donald Trump working on his constituents viewpoint. Great job
@slanejohnston
@slanejohnston 2 года назад
Very thorough, thank you, gotta do my gals "pretty lil" Prius. Keep her happy, and my wallet not so slim. Times is a gitting 'ruff out there..... Thanx guy..... You from up Jersey way?
@stacydornan9765
@stacydornan9765 2 года назад
Need a puller,airhammer and abfh
@thebush-craftingcousins2849
@thebush-craftingcousins2849 3 года назад
I don’t think it should’ve been that easy to get the axle nut off
@spelunkerd
@spelunkerd 3 года назад
Weekend warriers like us need to earn our tools. You certainly earned a few more tools with this job, good work! I'd start with a good set of jack stands, it's a scotty kilmer job with only a jack.
@Valient6
@Valient6 4 года назад
Machine that hub assembly seat face 3 thousandths over!
@Valient6
@Valient6 4 года назад
Smash that cast aluminum!
@sjoboo
@sjoboo 4 года назад
Thanks a lot! It made me decide to do this myself in stead of taking it to a shop.
@AllThingsBoost
@AllThingsBoost 4 года назад
Just did mine, I had to resort to a 6 ton press, but it is all corroded like that because that's what aluminum does when it contacts steel.
@irunxboxlive916
@irunxboxlive916 4 года назад
wheel bearing ez, dont take the hub off like he did, take the 2 thick bolts out and hammer out the axle then unbolt and hammer the bearing out, its E Z, dont take off the bottom castle nut or steering thing
@nordicpride9708
@nordicpride9708 4 года назад
For anyone doing this be sure to check for sticky front brake pads and assure your tires aren’t contributing to noise. I did mine recently and it helped but the other influencing factor was cupped tires due to worn struts.
@descolero1
@descolero1 5 лет назад
@2:29 "wow thats very loose, just how like it!" lmao
@michael47lamb
@michael47lamb 5 лет назад
Decent job! Very inspiring. However, everyone ! Please be sure to torque the bolts on the new hub and use jack stands so you dont have a nasty accident while beating on things.
@gerhard5911
@gerhard5911 5 лет назад
Thanks for pointing out the jack stands and the torque. Both are very important details.
@TDCornwell
@TDCornwell 5 лет назад
Great video! Very useful for me & my adventure replacing the wheel bearing on my '09 Prius. A couple pf things that this video does not cover: 1. The shield around the speed sensor in the back of the bearing. I removed this with only a little trouble by first removing the entire yolk/knuckle assembly, then gripping the shield with a pair of Vice-Grips and whacking on the yolk while holding the Vice-Grips. 2. I found this bearing was very, very hard to remove. My Prius grew up in Upstate NY State where there are awful road conditions for a few months a year. Salt, sand, snow, cold temperatures, etc. This puppy was STUCK, and hammering on it was pretty useless. Ultimately, I took the entire yoke/knuckle off & was able to put the assembly in my vice, pointing down. Being careful, the jaws of my vice would fit just between the bearing assembly and the knuckle. I didn't clamp down with the vice, just used it to hold the yolk, while beating on the bearing. I put the four bolts in most of the way then, using an impact socket to buffer the hammer blows, I whacked the heck out of the socket, one at a time on each bolt. This ultimately did the trick. This bearing was far and away, the most stuck thing I have ever liberated. It was glued (corroded) in the yolk like nothing I have encountered. I practically soaked the thing in penetrating oil ahead of time and, after I got it apart, I could tell that the penetrating oil didn't touch the corrosion. It was super-stuck. I tried heat and pressure, using a propane torch and fitting a small hydraulic jack between the hub bolts and the frame. These may have loosened the bearing assembly, but I'm not sure. 3. One thing I learned from this was to use some non-hardening sealant, and anti-seize compound to reassemble this puppy. I think that this was the fifth front-end wheel bearing I have replaced on my '09 Prius (220K miles) and I hope the next time is easier.
@coryhartford1069
@coryhartford1069 5 лет назад
Getting that bearing out is a SOB isn't it? Good work sticking with it. Thanks for sharing your experience.
@nordicpride9708
@nordicpride9708 4 года назад
Usually only if the car spent any time in the rust belt. You do get some corrosion being that they are two dissimilar metals (aluminum knuckle/steel hub). But nothing a mini sledge can’t persuade.
@gerhard5911
@gerhard5911 4 года назад
@@nordicpride9708 Chicago area car...that definitely qualifies for rust with all the salt on the roads.
@tdok
@tdok 5 лет назад
At 38:30 you showed the ring. What is that ring for?
@regeorge179
@regeorge179 5 лет назад
Thank you gothard Schiller for this video it will help me to do my own car when future wheel bearings needs replacement.most appreciated.
@midnightsunturbo
@midnightsunturbo 5 лет назад
Thank you for uploading the video. This will help me out when I need to replace mine.
@IgorKadulenkov
@IgorKadulenkov 5 лет назад
Great video! Thanks for sharing!
@JL-ut6lo
@JL-ut6lo 5 лет назад
Good job. A suggestion next time, instead of whacking the wheel bearing with a sledge hammer, why not leave the cap bolts loosely in (unthreaded say about 1/4 inch) and then strike at the bolt heads with a drift punch. By alternating from one side to the other, you can then "walk" the bearing assembly out of the spindle hub assembly. You might also be able to do this while the spindle is still attached to the strut. This way you don't have to do an wheel alignment at the end. Cheers!
@gerhard5911
@gerhard5911 5 лет назад
That's is a great suggestions. Thanks. I should finally get myself a press. Would make it much easier.
@TDCornwell
@TDCornwell 5 лет назад
This method (sort of) worked for me. Nothing else did. I took the entire yoke /"knuckle" off & was able to put the assembly in my vice, pointing down. Being careful, the jaws of my vice would fit just between the bearing assembly and the knuckle. I didn't clamp down with the vice, just used it to hold the yolk, while beating on the bearing. I put the four bolts in most of the way then, using an impact socket to buffer the hammer blows, I whacked the heck out of the socket, one at a time on each bolt. This ultimately did the trick. This bearing was far and away, the most stuck thing I have ever liberated. It was glued (corroded) in the yolk like nothing I have encountered. I practically soaked the thing in penetrating oil ahead of time and, after I got it apart, I could tell that the penetrating oil didn't touch the corrosion. It was super-stuck. I tried heat and pressure, using a propane torch and fitting a small hydraulic jack between the hub bolts and the frame. These may have loosened the bearing assembly, but I'm not sure. One thing I learned from this was to use some non-hardening sealant, and anti-seize compound to reassemble this puppy. I think that this was the fifth front-end wheel bearing I have replaced on my '09 Prius (220K miles) and I hope the next time is easier.
@DrEarbuds
@DrEarbuds 6 лет назад
Does it matter which brand bearing you buy
@gerhard5911
@gerhard5911 5 лет назад
depends on how long you want to keep the car running well. If its an older car. no
@DrEarbuds
@DrEarbuds 5 лет назад
@@gerhard5911 my Chinese mechanic use a jackhammer to loosen it up
@RAMRA10
@RAMRA10 6 лет назад
Did you ever get a metallic taste in your mouth after doing this job? Because I did. I used a simple dust mask. Should of used a better mask for the job.
@LostinCynicism
@LostinCynicism 6 лет назад
Stroke probably
@gerhard5911
@gerhard5911 5 лет назад
no, I didnt
@sungn4512
@sungn4512 6 лет назад
Good job in diagnosing & tackling problems with front wheels; some observations: - you are a MONSTER & a force to recon with the mini sledge hammer!!! whack... whack... ; ) - dust shields mangled and all - i normally liberally spray brake clean lubricant also helps in cleaning metal parts. - normally liberally Spray lubricant to help loosen metal parts to unscrew - are you ready to upgrade to a work bench & vice assembly? - I noticed that you didn't use a jack stand to suspend your car; its only a problem when there IS a problem. - Loose front wheel causes can be of various causes: - BEARING HUB. this is definitely the MAIN cause of your road noise, speed, pull. - LOOSE AXLE NUT, you noticed that loose nut immediately off the bat when you unscrewed it off the axle. It normally is ~170lbs torque, you took it off with about 30lbs of effort. I assess that you did some work on that axle as of recent that caused it to relax its tension. Probably need lock tight the nut back to seat in. - BALL JOINT. this also may cause your wheel to click - nice looking Prius - thanks for sharing your project
@gerhard5911
@gerhard5911 6 лет назад
Yes, you are correct. Just know, I did spray the day before. And no, didn't want to come out. I have a press at my shop which I normally would have used. But the monster in me just wanted to get the job done. The axle nut did come off at less the 170. Great observation. If I remember right I may have loosened them before filming. Ball joints checked out. If you would have heard the extremely loud grinding noise you would have been shocked. I even thought there was something wrong with the drive train after replacing the loose left side and the noise was still present. After the repair was done I knew for certain in THIS case it had been the wheel bearings. But when I started I was about only 80% sure. Thanks for the comments. I am aware that there are some more refined and elegant ways to do this job, no doubt. And thanks for reminding me for not becoming sloppy on the blocks. After all I had the jackstands right there.