Yes sir, but this video isn't the best example. This one has better gyroflow stabilization ru-vid.com/video/%D0%B2%D0%B8%D0%B4%D0%B5%D0%BE-iklVh8Tv3W4.htmlsi=ru6e7-4ORqwu8vWs
Hey I tried this with a full hero 11 and brand new cinebot30 stock pids. It flies perfectly fine, but I'm getting crazy vibrations/jello in the gopro. How did you fix this?
I'm sorry to read that, I honestly don't know what your problem is, I didn't change anything. My drone is in default pids and tune, maybe Try loosening the anti-vibration base screws a little, are your props okay? no scratches?
I am really considering trying a similar setup with my 6" quad for a YT Video... I am not quite sure if my 2806.5 1300KV Motors can lift my a6300 with a similar lens, but I think I'll try... Did you use FC Gyro data to stabilize with Gyroflow? Also: How did you mount the camera? Just with a 3D Printed mount, ball head, or just screwed on? I would really like to talk about that setup some more, maybe on Instagram?
I think 1300kv is a little low, the sweet spot for it will be 1500 to 1700kv, I use the gyro data from the o3 Air unit in this video but the gyro for the FC works too, the camera is hard mounted and secured with battery straps, hit me a dm on ig and will send you a photo of this setup @chrisvsgravity
Hi man! Awesome video! Do i understand correctly that you have mounted the Go Pro hero 11 on the Cinebot 30 with this one "GEPRC CineLog35 FPV Camera 10"? Does Hero 11 fits in the mount for 10? Thanks! <3
Please help, My cinebot30 can’t handle the full gopro with 6s 1050mah batteries, anyone have an idea why? Does it need to be fine tuned or not? I ordered from Geprc offcicial website
Please help, My cinebot30 can’t handle the full gopro with 6s 1050mah batteries, anyone have an idea why? Does it need to be fine tuned or not? I ordered from Geprc offcicial website
Great moves! May i know the PID Tuning? I have a similar drone with yours but the tuning seems very bad at some point. I have a video when it goes bad behaviour from the drone in my channel if you want to see
I already saw your video and I also have the default PIDs from GEPRC, what is happening with you is very strange, do you try fly in acro without air mode?
@@ChrisvsGravity Thank you for your reply. I’ve found the problem. The wobble come is from the overheat motor. So, i turn it down the filter. Now, the wobble is gone and motor is not heat anymore