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I STARTED MY 300ZX FOR THE FIRST TIME IN 9 YEARS 

Josh Charlton
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Welcome to the 2nd instalment in my abandoned 300ZX rebuild series! In this video, I'm going to attempt getting it started after 9 years of sitting untouched on a driveway. Something tells me this project is going to take me quite a while...
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joshcharlton13
joshcharlton13
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I do not own/do not claim to own any of the music used in this video.

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5 сен 2024

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Комментарии : 36   
@yesii2340
@yesii2340 Месяц назад
Good to see she's alive! Don't stress about the head gasket, the engine bay is very overwhelming but once you take its makeup off its not actually too bad.
@Joshcharlton13
@Joshcharlton13 Месяц назад
Rusted bolts im finding are my worst enemy 🥲 the next episode is going to be a very long one I think
@vecanis
@vecanis Месяц назад
Welcome to the joys of Z ownership. Hopefully you have a good place to pull the motor and place it on a stand so you can strip it down. Runs really well despite the bad head gasket.
@aaronsmyth3763
@aaronsmyth3763 Месяц назад
Looking much better than before. Congrats on getting it running 🎉
@Joshcharlton13
@Joshcharlton13 Месяц назад
It’ll look even better when it runs 😮‍💨 Thank you mate 🙏
@recyclerize
@recyclerize Месяц назад
Glad your most importantly enjoying the ups and downs of cars, with all the head scratching moments the rewards are brilliant 😊😊
@Joshcharlton13
@Joshcharlton13 Месяц назад
Couldn't agree more! The end reward will be well worth the effort I’m putting in now 💪🏼
@gateaccess818
@gateaccess818 Месяц назад
you got this!! not easy, but not hard either!
@Joshcharlton13
@Joshcharlton13 Месяц назад
Going to give it my best shot! Thank you mate 🙏
@vincenthanna2162
@vincenthanna2162 Месяц назад
Great vid. I had a similar issue with one exhaust was clear but the other was smoking. We took it apart it was piston rings. Good luck with build.
@vincenthanna2162
@vincenthanna2162 Месяц назад
I have a 1989 300zx tt swb t top manual. It’s mint.
@Joshcharlton13
@Joshcharlton13 Месяц назад
I didn’t even think about the piston rings… but now you mentioned it I’ll definitely check them all out when I get to them 👀 Thank you mate!
@vincenthanna2162
@vincenthanna2162 Месяц назад
@@Joshcharlton13 Also check exhaust valves. That can cause smokey exhaust.
@gateaccess818
@gateaccess818 Месяц назад
on first start with fresh petrol it dosen sound as if need new spark plugs or injectors do need some time running with a cleaner through the gas tank so all carbon / rust can be cleaned off the injectors and they can have a clean and even spray pattern
@M.TTT.
@M.TTT. Месяц назад
At fist I thought you owned it and let it sit for 8 years, but I see its a project car you bought. Good save
@gateaccess818
@gateaccess818 Месяц назад
@11:50, great way to flush all the rust out of the system. like a gieser lol, hope no one badly burned.
@gateaccess818
@gateaccess818 Месяц назад
first start in 9 years, def bad fuel and youre lucky!!! most cars sat that long have injectors that are all stuck, and fuel hanger all rusted out frm fuel spoiling. i had a customer car sat for 7 years, tank was so rusted the wires off the pump fell off the hanger and were free floating live power inthe tank. i was wondering why it wouldnt prime. scary shit. thankfully all fixed now. even the rings in the piston were frozen in place so compression was shit, i let atf sit in cylinders for a week, that plus hand cranking motor freed rngs, had to clean injectors. finally got motor runing good. took so many systems being serviced or replaced.
@gateaccess818
@gateaccess818 Месяц назад
100k kil. low odometer. nice score homie
@Joshcharlton13
@Joshcharlton13 Месяц назад
I believe it’s 100k miles… but still not bad for 31 years old 👀
@gateaccess818
@gateaccess818 Месяц назад
bro youre rear spoiler is rare as fuckkkkkk, thats MONEY!!
@Joshcharlton13
@Joshcharlton13 Месяц назад
Apparently it’s a Monza spoiler… whatever that might be 🤷🏼‍♂️ Definitely keeping it on!!
@awaisdon2868
@awaisdon2868 Месяц назад
Really looking forward to the next episode. Also always connect the positive before you connect the ground. It didn't short out because you left the ignition on
@Joshcharlton13
@Joshcharlton13 Месяц назад
Thank you mate! Yeah massive rookie mistake 😂
@destruct61
@destruct61 Месяц назад
It wasn't that you left the key in the ignition or even on you connected both the positive and negative terminals at the same time and tried to tighten them The proper way is to put the positive cable on first and tighten it then do the ground you will never have that happen
@Joshcharlton13
@Joshcharlton13 Месяц назад
Someone else told me that... which in hindsight makes a lot more sense 😂 Something to avoid next time
@lbx-1581
@lbx-1581 Месяц назад
She liiiiivvvvvvveeeeesssssss! Taking down the engine will be interesting. You can pull it off mate 💪
@Joshcharlton13
@Joshcharlton13 Месяц назад
Thank you mate, it’s going to be a learning experience for sure 👀
@thefergusonlover5898
@thefergusonlover5898 Месяц назад
She’s aliveeeee
@Joshcharlton13
@Joshcharlton13 Месяц назад
Like one of Frankenstein’s creations 💀
@gateaccess818
@gateaccess818 Месяц назад
head gasket job, sorry. but worth it.
@NurseMjVery
@NurseMjVery Месяц назад
Great sir
@wishybishy
@wishybishy Месяц назад
Are you completely sure the wet bank is head gasket related? I'm asking because I'm having mine worked on at the moment. I've ended up buying new injectors, coil packs, new plugs (the list could go on) but the garage working on it are adamant my head gaskets are fine yet my exhaust is wet too on the same side. It's ultimately running too "rich" at the moment and pushing out more fuel to air ratio. My 300 project has been paused for now, but only because the garage that has it also build race cars and they've taken priority more recently as it's season
@Joshcharlton13
@Joshcharlton13 Месяц назад
I'm 100% sure it's the gasket, there is literally no other way it couldn't be. If you've bought all of that stuff and it's still wet I could only suggest the gasket and the garage are trying to swerve the job, as it's an absolute pain in the backside. Have you done a compression test of chemical test from the radiator? That should tell you right away whether or not the exhaust fumes are being pushed back into the rad... which means you have definitely got a blown gasket. They're not expensive to buy and will tell you right away:)
@wishybishy
@wishybishy Месяц назад
@@Joshcharlton13 This is what I've currently had done: •New injector set (370cc) •New injector wires •Set of new coil packs •New NGK Platinum Spark Plugs •Smoke tested •Pressure tested •Silicone hose kit (Silicon Coolant Pipes / Silicone Booster Pipes / Silicone Breather Pipes / Silicone Ancillary Pipes) •Auxiliary Belts (2) •New Thermostat •New Mishimoto Radiator •Coolant flush and top up •Vacuum Pipe O' Rings •Reset TPS to 0.48v and adjust idle speed to 750rpm •Complete Head Gasket Kit (not all of it was used) •Throttle Bodies balanced Plus a host of loosening and lubricating of other components too. All other wires have been tested for corrosion but are fine. Despite all of the above, it continues to run too rich on idle only. But the moment it's revved, it instantly disappears. There's no performance air filter on, only the standard air box. The garage is more than prepared to do any job that's required, but only if it needs doing in the first place.
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