A day out to test after suspecting that the old stubby antenna was damaged internally. Swap that for a Foxeer RHCP 5.8G stubby omni to see how good and far the video quality is.
Secondly, because the last test on the video quality failed, to my standard, due to the fact that it was interfered by some 5.8G signals at the Marina roundabout, i decided to put in a preflight check routine using one of the features of my IRC Rapidfire module that I mounted onto my Digital goggles via Video input.
Thirdly, I just reduce the filtering using the explanation by Chris Rosser so that I can have less latency which will improve the propwash handling of my Nazgul5 v1 (old Hardware with new Firmware). Doing some quick moves to flow around the trees while observing if I need to improve the propwash handling even further.
0:00 Introduction - reference to previous video showing bad VTX
2:41 Pre-flight check - scan for interference
4:29 Change Analog VTX channel
5:01 Maiden flight
9:27 Post maiden flight analysis
10:12 Check Gyro scaled and filtered noise
10:46 Longer distance video test flight
13:03 Stressing the motors a bit more
16:02 Betaflight Settings
This Build:-
Build : Nazgul5 V1 original parts
Camera: Caddx Ratel 1.66mm lens
Props : Ethix S4 Lemon Lime
Action Cam : Runcam5 Black
Lipo : 4S - 1550mAh 100C, 1500mAh 120C and 1300mAh 95C
VTX antenna : Foxeer Omni Stubby RHCP
receiver : R9 slim+ with ExpressLRS FW 2.5.0
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#Nazgul5
18 апр 2024