Тёмный

Polaris Magnum 325 Fuel Starvation Fixed! - Running Lean | Not the Carb & Not the Fuel Pump - Part 2 

ProjectTimeGarage
Подписаться 19 тыс.
Просмотров 62 тыс.
50% 1

Find out why this Polaris Magnum 325 is starving for fuel, running lean and backfiring. It's not the carb, not the fuel pump and not what I thought!!
***Links to products I use, or are seen in the video***
• Polaris Carb Boot: amzn.to/3Cdouxe
• Polaris Air Cleaner: amzn.to/2VuKPFk
• Polaris Carb Rebuild Kit: amzn.to/3DtR51R
• Polaris Fuel Pump: amzn.to/2WJx5Hs
Follow us!!
Instagram: / projecttimegarage
Facebook: / projecttimegarage
Looking for Merch? project-time-garage.creator-s...
E-mail us:
projecttimegarage@outlook.com
Our mailing address is:
Project Time Garage
1113 Murfreesboro Rd
Suite 106 #109
Franklin TN 37064
DISCLAIMER: Links included in this description might be affiliate links. If you purchase a product or service with the links that I provide I may receive a small commission. There is no additional charge to you! Thank you for supporting this channel so I can continue to provide you with free content each week!

Опубликовано:

 

2 апр 2021

Поделиться:

Ссылка:

Скачать:

Готовим ссылку...

Добавить в:

Мой плейлист
Посмотреть позже
Комментарии : 192   
@thomaslietz7035
I really like how you go through these videos so let me start off by saying thank you and I also wanted to let you know that’s the reason why it ran better when you put the air filter box back on it’s because that’s where your vacuum goes from your engine block that helps with the vacuum for you’re fuel flow so you have to have that put on for the fuel pump to work properly
@jontrenthem3751
@jontrenthem3751 2 года назад
After watching many videos, this one helped me with my Sportsman 500 . I put the cover over the filter and it made a great difference.
@basilhouse7937
@basilhouse7937 3 года назад
Thanks so much , I am resurrecting the same Machine here in Adelaide Australia . What an awful machine to work on , took me 2 hours to get the carby off . Your video has been a great help , and I no longe4 feel an idiot in taking so many parts off to get to the carby . Let’s hope when I get the unit fixed it will catch fire in the next fire season and save me working on it again . Thanks again , really great video .. Richard , south Australia
@theofficial_hunt
@theofficial_hunt День назад
This video just saved me ripping everything apart! Already been through the gas, spark ect. now I found both boots bad! Thank you!
@cootersgarage4408
@cootersgarage4408 3 года назад
Thanks man. My 2001 Polaris trail boss 325 is having the same problem. After I posted a video yesterday about mine and asking for help, today, I found your video. Lol. New stuff on the way.
@stevegiroux239
@stevegiroux239 Год назад
I was amazed when you found out that it was the carburetor boot to the main block the boot had a small crack that was not noticeable until you sprayed it and seen the fluid disappear into the boot I’m glad you were able to correct it and that you noticed that the air filter had to have its main cover on to allow a certain amount of air flow to allow the carburetor to run just right.
@aretemotors2205
@aretemotors2205 2 года назад
thanks for putting this out there! I ended up having the exact same issue and your video saved me a ton of time!
@tomnovak7731
@tomnovak7731 2 года назад
I love how you go through all that and in the summary you don't mention the part that was actually bad! Your main problem was the boot between the carb and the engine.
@user-pe7ue5pe5t
@user-pe7ue5pe5t Год назад
You said you didn't know why they use a fuel pump it's just for safety shuts the fuel off if flipped or an accident. Your video fixed my quad. Just needed air box lid. Thanks for the video
@stevegiroux8943
@stevegiroux8943 2 года назад
I liked the way you fast forward yourself putting it together lol 😂
@mattemkow
@mattemkow Год назад
Great videos! I love the details and have been troubleshooting a 1999 Sportsman 500. This was vary helpful and shared the same issues with the air box resulting in a good mix when off and too rich when closed. I chased my tail for weeks and your video helped me figure it out. Thank you.
@wheatwear
@wheatwear 2 года назад
Great video! Excellent job of editing! I've seen many videos where the subject title is focused on the problem but the video goes off on tangents not staying focused on the problem. Cheers from the Finger Lakes!
@phil9171
@phil9171 2 года назад
I just got my Polaris 4x4 magnum 425 back up and running. I'm running into the same issue. Glad I found your video. Will look at that inlet that goes into the head to be sure it is sealing good and the clamp that goes on the carb from that inlet, then the airbox. Dang temper mental Polaris!!!
@lylekime
@lylekime Год назад
have the same problem thanks for the video
@clemanderson6364
@clemanderson6364 2 года назад
I have the same problem so this film was excellent thank you for doing them.
@marquslams3451
SOMEONE WAS IN THERE WITH YOU IN THIS REPAIR. THEY MOVED THE GEAR SHIFT STICK.
@StevenHannan-zo7gt
Looks fantastic I just found one of these behind my neighbor's shed. She wants to sell and I need a frustrating project in my life 😂 I can only hope it turns out as good as yours. Thanks for the inspiration.
@georgehirvela7435
@georgehirvela7435 Год назад
Thanks, man, that's what it was for mine also, the damn air box cover....
@thomasunger8774
@thomasunger8774 Год назад
I have successfully bypassed the fuel pump on 4 polaris atvs simply by taking the fuel line to the pump and running it directly to the carb. Gravity flow just like a Honda and it works great.
@mattclark7748
@mattclark7748 3 года назад
great detective work. your good at that
Далее
Редакция. News: 128-я неделя
57:38
Просмотров 1,3 млн
Бмв сгорела , это нормально?
01:01
2002 Polaris Magnum 325 carb rebuild
51:40
Просмотров 39 тыс.
Polaris magnum 325 carb clean and new starter
26:05
Просмотров 3,8 тыс.
Changing oil on Polaris 325 Magnum 4x4
6:53
Просмотров 18 тыс.
Motorcycle and ATV Carburetors 101
22:42
Просмотров 417 тыс.
2004 400 sportsman carb bogging fix
21:33
Просмотров 88 тыс.