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Seller Said This Dirt Bike Has a Horrible Bog 

2vintage
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I buy a 1995 Honda Cr250 dirt bike with a bad bog. Let's fix it. #Honda, #2stroke, #Fix,
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The following video features activities performed in controlled environments by knowledgeable persons. DO NOT attempt to duplicate, re-create, or perform the same or similar activities at home, as personal injury or property damage may result. 2vintage( Joe Weber, the persons shown in this video and ANY CONTRIBUTOR, ARE NOT LIABLE FOR ANY such injury or damage. ALL 2vintage( Joe Weber) CONTENT IS FOR ENTERTAINMENT PURPOSES ONLY.
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25 июн 2024

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Комментарии : 1 тыс.   
@-Sunny--
@-Sunny-- 2 дня назад
This channel is like meditation for men!
@rhamog8548
@rhamog8548 2 дня назад
Damn rite ay brother
@ajc5370
@ajc5370 2 дня назад
F yeahhhhh with a Coors in each hand! Therapy !
@leedimatteo5078
@leedimatteo5078 2 дня назад
brother!!
@Ajaxaxxess
@Ajaxaxxess День назад
Need to light those 2 stroke scented candles to really feel the vibe!
@seanoxborough5830
@seanoxborough5830 День назад
Weird,
@qacomputers3344
@qacomputers3344 2 дня назад
spray starting fluid where the JB weld is while holding the throttle at a steady RPM and see if it revs higher due to a leak and sucking air...
@minnesotatomcat
@minnesotatomcat 2 дня назад
Yes I was gonna suggest the same, I use that trick on vehicles all the time to find vacuum leaks. I’d spray it around the carb too, could be a crack in the intake boot or anything else, that’s a pretty old bike now.
@ajc5370
@ajc5370 2 дня назад
Great idea and quite honestly is a pretty easy fix to depending. A good TIG welder can button it up quick if it's not terrible
@tuberNunya
@tuberNunya День назад
The intake doesn't suck air from the crankcase, Mr Mechanic.
@oriancunningham
@oriancunningham День назад
@@tuberNunya youre trolling, a bad seal, or small crack in the case would cause a vacuum leak
@PurpleMonkeyWaffle
@PurpleMonkeyWaffle День назад
If it was sucking in air then fatting the jets would have helped. He went all the way down to 130 and still same problem.
@stevefirth6472
@stevefirth6472 2 дня назад
Before you tear anything down, check the power valve. That's what it sounds like to me.
@tjanusz3
@tjanusz3 2 дня назад
first thing i thought
@randomboxguy9320
@randomboxguy9320 2 дня назад
thats what i was thinkingtoo
@lucascady4992
@lucascady4992 2 дня назад
Same!
@annone6462
@annone6462 2 дня назад
Yep, gotta be the ol’ power valve. Free her up. (I have no idea, just agreeing)
@eltonwhite8490
@eltonwhite8490 2 дня назад
I was thinking the same thing
@OldmanADV
@OldmanADV 2 дня назад
check pipe , to make sure there is no obstruction ! I had this issue with a 2001 cr250
@DavidPhelps-du1mx
@DavidPhelps-du1mx 2 дня назад
Could bent places in pipe have caused an airflow restriction? Spark arrestor plugged?
@HenkkaEuro
@HenkkaEuro 2 дня назад
@@DavidPhelps-du1mxdepends on where on the pipe its located
@bruceprosser4283
@bruceprosser4283 2 дня назад
Agree 110%.. When you pulled the plug the first time and it was wet, I said pull the pipe and check for oil residue. I have had to clear out a CR 250R pipe by burning it out with a propane torch. It did the trick. Peace
@Yz4Life
@Yz4Life 2 дня назад
And re pack the silencer!!! Every 20 hours is the spec in most manuals, the packing degrades and gets soaked with oil inhibiting the top end of the power band
@HenkkaEuro
@HenkkaEuro 2 дня назад
@@Yz4Life fax
@arrobrewer2730
@arrobrewer2730 2 дня назад
I'm amazed at how many times you miss 2nd 😊
@zOrO2kX
@zOrO2kX День назад
Every single time. It's like a trademark.
@dougaranda6187
@dougaranda6187 2 дня назад
Since re-jetting didn’t have much effect, I wouldn’t rule out electrical just yet. Just because the spark plug checker shows a plug is ok, that doesn’t mean the other components aren’t breaking down.
@anthonyjacobs8773
@anthonyjacobs8773 2 дня назад
Excatly what I was thinking. Does that look like a tape job coming from the stator wire?
@2strokeme64
@2strokeme64 День назад
Cracked stator plate, throws it out of time at higher rpm, figured this out on a banshee, only after countless hours fukin with dual carbs....
@PurpleMonkeyWaffle
@PurpleMonkeyWaffle День назад
I'm thinking the flywheel has gone bad. He needs to check if there is fuel in the exhaust. If so the ignition system is faulty.
@PurpleMonkeyWaffle
@PurpleMonkeyWaffle День назад
@@anthonyjacobs8773 I recently had a loose coil wire its more like a complete loss of power than a backfire then FULL power then no power, backfire etc. I've also had bad flywheel which was very similar to this.
@JonRoundtree-mu5gb
@JonRoundtree-mu5gb 2 дня назад
Mid range bog=power valve sticking or misadjusted. Set the power valves up right and try a 170-175 jet. You should solve it that way.
@franksando635
@franksando635 2 дня назад
A walk around with our Vinny is just not right 😂
@fordfan6474
@fordfan6474 2 дня назад
I do believe that dog spends his time stuck in kennel sad if u ask me, mine would of just hoped out the truck after we got home with the new toy, joe rarely includes Vinny…..
@carltreurnich8482
@carltreurnich8482 2 дня назад
Power valve?
@allan9603
@allan9603 2 дня назад
​@@fordfan6474 We miss the Vinster!
@allan9603
@allan9603 2 дня назад
​​@@fordfan6474I think Vinny may have gotten paddled and is on restriction 😅😂
@ferdivanderberg2493
@ferdivanderberg2493 2 дня назад
Power valves or clocked exhaust
@mikespak1473
@mikespak1473 2 дня назад
Do a crankcase leak down test, check power valves and check for exhaust restriction.
@dixoncider7256
@dixoncider7256 2 дня назад
You know what's up! 👍
@travisconover4762
@travisconover4762 2 дня назад
My buddy's yz 250 sounded like that, and to find out it was a partially clogged silencer.
@steveaustin1984
@steveaustin1984 2 дня назад
Take your pick of which to tackle first: 1. Crank seal 2. Power valve 3. JB weld
@stkyfngrszmooth
@stkyfngrszmooth 2 дня назад
I'd go with the power valve first only because I had this same exact issue with my '90 YZ 125. Turned out the mechanic reassembled the bike with the power valve backward. After fixing the issue, it was business as usual, with the bike revving out with zero hindrance.
@michaelesposito6678
@michaelesposito6678 2 дня назад
3 first 2 second tear down 3rd
@Proxiir
@Proxiir 2 дня назад
Could definitely be a sticking power valve or air leak.
@louieuribe3343
@louieuribe3343 2 дня назад
Leak down test… that will narrow it down quickly. All the carb adjusting in the world won’t fix the issue if there’s an air leak. Good luck and keep up the great work and content.
@brendans7489
@brendans7489 2 дня назад
definitely a crank seal i think, my 250r did the same thing.
@1bennyfred
@1bennyfred 2 дня назад
Just fought a similar battle on a 2000 KTM with a Keihin carb. Hours of swapping jets. Long story short, it was the carb. Found an OEM (not Chinese replica) and it instantly solved the problem.
@Skis878
@Skis878 2 дня назад
lol thats what you get for playing with chineseium
@viniciuswiermann3010
@viniciuswiermann3010 2 дня назад
@@Skis878 Kei hin carbs from that era are 100% japanese tho
@michaelgarland579
@michaelgarland579 2 дня назад
Same with my yz125 2003 the carb was bad it had mukui junk so I bought lectron carb now it runs strong 💪 that an apex head its awesome best thing I did to the bike an new piston numura pistons are really strong 💪 I had wiseco burn up an melted ring mess up my cylinder so I been using numura pistons they are good
@craigmorgan4676
@craigmorgan4676 2 дня назад
Chinese 1s no good then brother?😬🤔😫😫👎👎👎🤝
@rogermayer6131
@rogermayer6131 2 дня назад
Do a pressure / vacuum test to test the crank seals .
@just4kicks950
@just4kicks950 2 дня назад
IMO it's pulling air from the crank seals. I would inspect the case for cracks because of J.B weld deal. Joe sweet bike overall 🎬🔥👍🫡
@idahoduckhunter
@idahoduckhunter 2 дня назад
Learned about that issue from Jennies Garage
@gutsngorrrr
@gutsngorrrr 2 дня назад
This was one of my all time favourite bikes I've owned.
@countrygaming8367
@countrygaming8367 2 дня назад
It’s favorite 😊 this word is commonly misspelled
@gableroux136
@gableroux136 2 дня назад
@@countrygaming8367 Both grammatically correct... just like color and colour.🙃
@okbommer8489
@okbommer8489 2 дня назад
@@gableroux136 u took down countrygaming 😘
@gableroux136
@gableroux136 День назад
@@okbommer8489 That's a victory in my book!
@jasonblankenagel5412
@jasonblankenagel5412 2 дня назад
Since the bog is at the mid to upper RPM's only, It would likely be an obstruction in air flow. Check Power valves to make sure they are fully opening at the higher RPM. Also, make sure your pipe and muffler are clear.
@dixoncider7256
@dixoncider7256 2 дня назад
👍
@Wantobefit
@Wantobefit 2 дня назад
You beat me to another bike, had this one saved on Market Place myself and was pondering about purchasing. Awesome find and enjoy the videos.
@MrGeoffrobodine
@MrGeoffrobodine 2 дня назад
I remember when I could read jet #s without using glasses a flash light and magnifying tool. 😂😂😂😂😂
@brainstain22
@brainstain22 День назад
How old are you?....Just wanting to know when to expect it...😂
@MrGeoffrobodine
@MrGeoffrobodine День назад
@@brainstain22 I'm almost 60... starts in your40s
@brainstain22
@brainstain22 День назад
I'm 42 this year....lol. Damnit....I'm getting old. 🤣
@martindavis925
@martindavis925 10 часов назад
I’m 63 and need all those tools to read tyre sizes nowadays 😢😢
@DealinDmg
@DealinDmg 2 дня назад
Joe you finally bought a bike that stumped. You will never accept defeat. All your viewers know that. So I'm looking forward to your next video. I'm curious on what the bike needs to be done to correct the issue.
@2vintage
@2vintage 10 часов назад
video coming soon!
@shawnlowell4522
@shawnlowell4522 2 дня назад
Check you harness grounds , ohm out your coil ..even cleaning your fly wheel an make sure it set right , I think its electrical
@2vintage
@2vintage 10 часов назад
I will check
@f.catfracassofracasso404
@f.catfracassofracasso404 2 дня назад
Check the power valve see if the last owner played with the settings in the power valve. You can adjust it to open sooner or later on the cylinder there is a stamp that says H and L check to see the position.
@rickoshea2114
@rickoshea2114 2 дня назад
Did you check that ground where the frame was painted
@thebigguy8306
@thebigguy8306 2 дня назад
Ol' Joe loves his dirt bikes. Nice looking cycle, a very popular/big seller, now let's tear it apart. Lots of teaching/learning moments
@1911MikeinOregon
@1911MikeinOregon 2 дня назад
I REALLY like that bike... I can see why the previous owner was frustrated with it. Like you, I would have started with the carb, but after seeing the air screw only turned out 1/4 turn and inspecting the carb, I would have checked the power valve. I would certainly check it before resorting to completely tearing down the engine because it has decent compression and visually everything looks good.
@ronsherfy6291
@ronsherfy6291 2 дня назад
Do a leak down test first and while doing so spray soapy water around the jb weld case repair. Check power valve for excessive carbon build up or possibly worn or broken power valve. Silencer may need cleaned and re packed. Clean up all ground contact points on the frame. Had a bike years ago with a bad port job done by a goon that acted just like this. Rule out the above mentioned before tearing it down. Good Luck! It’s a good looking bike!
@staygold902
@staygold902 2 дня назад
I've said that many times. It's critical to leak test 2 strokes. He's not once done one on video. Never
@jakeowens1770
@jakeowens1770 2 дня назад
Word up on the power valves. Had that same problem. Don't think its vacuum case issue as the plug would be white
@staygold902
@staygold902 2 дня назад
@@jakeowens1770 he has no idea what the plug is actually reading he didn't do a plug chop
@jakeowens1770
@jakeowens1770 2 дня назад
@staygold902 if it had vacuum leak, it would run better with more fuel and higher main jet.
@staygold902
@staygold902 2 дня назад
@jakeowens1770 depends how bad it's leaking and he only tried one larger jet It's nothing to go to the hardware store and fab up a leak tester. Fresh rebuild should have it done every time. He's never done one in his life. It's necessary. You can't rule out something you haven't even checked. But I agree something could be going wrong in the power valves too. Might have to check lol
@jeffmckc2081
@jeffmckc2081 2 дня назад
Those spark checker can be a simple check but they have no combustion chamber pressure on them so don't rely on it completely or it can bite you
@poorsob
@poorsob 2 дня назад
If this year still has the exhaust power ports, they might be carboned up and sticking. Definitely worth cleaning those and putting stock jets back in. Check the muffler packing too. I have a 1989 that I bought new. Still runs like a champ. Original everything if you can believe it. I love it!
@gutsngorrrr
@gutsngorrrr 2 дня назад
Yep, agree on both possibilities. I've had the exhaust packing etc fall apart causing partial restriction with similar problems. I would have said the crank seals, but as seen, no signs visible.
@qacomputers3344
@qacomputers3344 2 дня назад
that's a good recommendation, I didn't think of that one,,, a good call,, but I still think its sucking air through the JB weld....hmmm?
@poorsob
@poorsob 2 дня назад
@qacomputers3344 Still possible but I think his jetting would have made a difference (hidden the problem)... maybe...maybe not. Tough one. Clean the exhaust port power valves. It won't hurt and it might fix the issue.
@chrisnelson380exc
@chrisnelson380exc 2 дня назад
@@poorsob
@TheHowitz
@TheHowitz 2 дня назад
Man i'm stoked you're making this video. I have a 97 that has a similar problem. I replaced the right side crank seal with no improvement.
@dixoncider7256
@dixoncider7256 2 дня назад
Just saw this comment a couple of lines below yours, "My buddy's yz 250 sounded like that, and to find out it was a partially clogged silencer"
@dixoncider7256
@dixoncider7256 2 дня назад
Read through all these video comments. Lots of great information. Here is another one, "Before you tear anything down, check the power valve. That's what it sounds like to me"
@benburton8463
@benburton8463 День назад
I know its not the crack seal. The bike would rev all over the place like high low tick overs takes ages for revs to drop down. Power valve or stator or coil, even a bad cdi
@leewaken5059
@leewaken5059 2 дня назад
Never cared for the "95" purple. I had a new 94, which was gorgeous. Either way, this was a nice score on your behalf.👍🏼 With some patience, this bike will return a hefty sum at some point. Detail the hell out of it and keep it in the showroom condition that it is.
@ajc5370
@ajc5370 2 дня назад
I never understood the purple at all??
@TheBababa420
@TheBababa420 2 дня назад
See what s up the JB weld.
@thebigguy8306
@thebigguy8306 2 дня назад
IMHO always a RED FLAG - run away
@user-md4ih8hg9t
@user-md4ih8hg9t День назад
Why can't jb weld fix it?
@PaulHigginbothamSr
@PaulHigginbothamSr 2 дня назад
If I had one a small hole would be much better than a crack, which will need drill at the ends to make sure it doesn't travel laterally.
@qacomputers3344
@qacomputers3344 2 дня назад
yep, the same thing when I repair cast water lines,, drill a hole on each side of the crack, tap the pipe till the crack reaches the holes, then clamp it...
@kellerchappell5046
@kellerchappell5046 2 дня назад
Just wanted to say that I love the videos Joe. I am 15 and have always had a passion for working on these machines. I have 2018 Suzuki drz 125l and I enjoy upgrading it. Ive been consistent watching for a few years and have picked up on quite a few things🤙
@jacobvermeulen666
@jacobvermeulen666 2 дня назад
My 2002 did the same thing it was Servo for my ev power valve.
@robprice6573
@robprice6573 2 дня назад
I would check that JB weld repair first see if air is leaking from engine
@karl6823
@karl6823 2 дня назад
I would go for the crank seals, after checking the power valves
@Pulkka_
@Pulkka_ 2 дня назад
Check the powervalve. The fact that 155 ran the best might indicate that that the jetblock gasket might be broken.
@jeffkovacs5974
@jeffkovacs5974 2 дня назад
Look at the baffle material in the silencer
@Killawife
@Killawife 2 дня назад
Lol! I once worked on a bike a whole afternoon before I realized it had a sidestand switch preventing it from starting. I had the carbs off, plugs out, battery charging and all.
@Deathtrap617
@Deathtrap617 2 дня назад
Pro circuit pipes work amazing on these bikes, I raced cr250’s from 1990 to 2008 the I switched to Yamaha 450’s
@mikenielsen8738
@mikenielsen8738 День назад
whats the diffrent between 250 - and 450 topspeed ? Iam 186 cm 150 kg and i didnt no is 250 enough power for my weight the bike is for fun and speeding and a bit enduro
@davidvaeyens2188
@davidvaeyens2188 2 дня назад
Vinny just called me and said...David please tell my owner...I am 1000% sure it is the ignition...CDI...coil...I don't want to be near the backfires..😊
@joebinder6119
@joebinder6119 День назад
Get a stock coil
@harrybosch5720
@harrybosch5720 2 дня назад
Yeah, Id think your chasing your tail with the jetting, I suspect air ingression thru the crank seals or that crack in the crankcase... somewhere its getting in. These faults are real buggers to solve but great when you nail it. At least you can shut the garage door on it and dont have to ride it home. Have fun!!
@gottamodify7756
@gottamodify7756 2 дня назад
52 pilot on these hondas is what we ran.
@julianp4787
@julianp4787 2 дня назад
JB Weld on cranckcase is letting in air. The higher the revs, the more it sucks in, the more lean the mix :)
@bwfreel
@bwfreel 2 дня назад
That’s what I thought, JB weld is a clue for sure
@greathornedowl3644
@greathornedowl3644 2 дня назад
Ding Ding Ding - I think that is the right answer
@nickgruber2593
@nickgruber2593 2 дня назад
Wow a CR! Nice 👍
@user-wn6el4rk5p
@user-wn6el4rk5p День назад
Nothing sounds better than a two stroke dirt bike in my opinion, actually anything two stroke!
@stkyfngrszmooth
@stkyfngrszmooth 2 дня назад
I've had this same exact problem with my 1990 Yamaha YZ 125. Turns out the mechanic put the power valve in backward. Once he fixed the issue, it revved out perfectly again.
@michaelesposito6678
@michaelesposito6678 2 дня назад
Mechanic)???? Lol
@stkyfngrszmooth
@stkyfngrszmooth 2 дня назад
@michaelesposito6678 He was actually a great mechanic. If you don't make a mistake every now and then, you're not doing enough.
@dixoncider7256
@dixoncider7256 2 дня назад
Good find.
@michaelesposito6678
@michaelesposito6678 2 дня назад
@@stkyfngrszmooth as long as he fixed it that's great
@michaelgalli8269
@michaelgalli8269 2 дня назад
Check the power valves
@Dismantledgarage
@Dismantledgarage 2 дня назад
I had a 93 same exact bike alot of good times on that machine!!
@CR250rSMITH
@CR250rSMITH День назад
$2000 for a bike that year, that good of shape is a DEAL
@GaryGilbertbigG66
@GaryGilbertbigG66 2 дня назад
Check the spark plug cap. Honda uses a resistor cap 5 ohms max. If ohms is 10 or higher with cause a retarder ignition. Also could be stator one coil runs the high revs after 5k rpms . In my opinion it's a timing issue. Cap is a issue I have come across many times. I am 58 years old. Been riding and wrenching for 50 years...
@rintin1874
@rintin1874 2 дня назад
Brilliant video Joe watching from Edinburgh Scotland UK 🇬🇧
@truthsetsyoufree77
@truthsetsyoufree77 2 дня назад
I reckon power valve sticking as its bogged hard at the beginning. I've had that happen to two yz 125's. If not could be the JB weld, or crank seals.
@CezaryAkakios
@CezaryAkakios 2 дня назад
When the jetting wasn't having much effect I was back to thinking ignition. Maybe check the gaps in the magneto pickups, the magnets in the flywheel, coil resistance, ignition module, etc. I could see one of those having an RPM dependent failure, such that it works fine below a certain RPM but then breaks up at higher.
@wiggie7420
@wiggie7420 2 дня назад
Power valve stuck shut
@BONNIECLYDE-1934
@BONNIECLYDE-1934 2 дня назад
Happy Days Joe Has Posted 🔥🔥🔥
@yeahright302
@yeahright302 День назад
sad,you need a life!!!
@tylerhosner9011
@tylerhosner9011 2 дня назад
I had a 96 kx250 that ran identical to that. It ended up being the power valves not functioning properly
@Aint9sk8rd9
@Aint9sk8rd9 2 дня назад
My 89 CR250 had a very similar issue and it was the power valves not working correctly. The power valves are a different setup on this but it's worth looking into.
@zachfarkash6430
@zachfarkash6430 2 дня назад
Love my 89CR250R great bike
@TN_HondaDad
@TN_HondaDad 16 часов назад
That is a VERY COOL spark plug tester!!! Never knew such a thing existed!
@rs5001988
@rs5001988 2 дня назад
My favorite Cr250 eva had a huge picture on my wall when i was a lad best look Cr in my opinion lovly nice score mate
@bret44
@bret44 2 дня назад
First thought when you pulled it off was the crank seals, they get hard and brittle after 20 years on a 2T. All that junk around the flywheel made me think it was blowing premix out on that side. I didn’t see any oil coming out the muffler so I don’t think it is the rhs seal. I guess it could be the power valve not opening.
@crazychad2720
@crazychad2720 День назад
2 stroke dirtbike go-to checklist for me when it comes to performance issues. *Jetting/Spark Plug *Reeds *Powervalve issue/dirty *Crank Seals -stator side will cause air to be. sucked in, causing lean condition. -clutch side will suck trans fluid into crank cavity making bike run very rich Usually one of these is always the cause, of a consistent performance issue. If it's intermittent, especially once warmed up, usually electrical. I see you touched these basis and took all the right steps.
@jakeallama22
@jakeallama22 2 дня назад
My first thought was power valves. Sweet looking bike! ‘93-‘95 are the best looking bikes Honda ever put out!
@benjones2895
@benjones2895 2 дня назад
Air filter is filthy
@johngarris8463
@johngarris8463 2 дня назад
Love your show man beautiful Honda keeping ripping
@charlie541
@charlie541 17 часов назад
Just had a bike with same symptoms. Chased the carb forever. Showed it to a pro mechanic friend, he told me to check the coil. That was it, I was shocked.
@snakeub9
@snakeub9 День назад
BIG FAN of the spark plug tester !!
@user-fi3fx5my2s
@user-fi3fx5my2s 2 дня назад
Kinda clanky kicking it over..
@larryburrough3024
@larryburrough3024 2 дня назад
Yo, dude. What is up with your granddaddy’s GoldWing! Don’t leave me hanging. Please ASK ME ABOUT THE DIAMOND PLATES!
@billycapshew2411
@billycapshew2411 2 дня назад
I been thinking the same thing
@atothez1931
@atothez1931 День назад
ive still been wondering about the tecate 3 he had.
@kootenaycat
@kootenaycat 2 часа назад
Check the power valves for sure, they need regular cleaning anyways. But my money is on a bad coil, it's breaking down at high rpm. If it had an air leak from that JB weld or flywheel side crank seal you'd think smaller main jet would make it worse. Looking forward to seeing the fix! Retired auto mechanic here but recently got into small engine stuff and enjoying the change!
@ECS46987
@ECS46987 2 дня назад
Love that year of CR. Great find.
@LukesRandomShit
@LukesRandomShit 2 дня назад
my money is on crank seals (due to smoke on first start) or CDI/spark related. It is like the issue i get with water on spark boot/coil grounding out the spark an or if the old cr has power valves being stuck closed.
@jakebrossard2878
@jakebrossard2878 2 дня назад
I just bought a 03 cr250 with bad bog! It ended up being the power valves were adjusted wrong. the servo motor wasnt opening the ports for mine at the right time. If this ytear has that motor, definitely worth checking! It still has the slightest bog at low rpm so i will be doing a carb tuning like this in the near future. great video, hope you find the cause on this bike, these things EAT!
@askfadzean
@askfadzean 2 дня назад
I have Lernt sooo much from watching you over the past few years Joe! you have solved Almost Every problem there is. Thankyou :) - Could your problem have somthing todo with the Pipe?/Chamber clogged?
@charlesgoss3521
@charlesgoss3521 2 дня назад
Not for this occasion, but for hard starting,and especially big bores, tilt the bike on it's side until you see gas overflow, put the bike in gear and rock it back and forth. Fuel is sucked into the engine and really helps promote firing. 2 strokes only, unless you want cam chain and valve timing problems. As a long term CR500 Honda owner and rider in all weather conditions, this really saves your right leg and all of it's components.
@MrKawie1001
@MrKawie1001 2 дня назад
I had this same issue with a 91 cr125r and i couldnt ever figure it out to the point i just sold it.
@jayjudd6518
@jayjudd6518 2 дня назад
That’s sad
@MrKawie1001
@MrKawie1001 2 дня назад
@jayjudd6518 o well got a 01 kx250 with the money from it so 🤷 win win someone got the cr they wanted and I got the bike I wanted
@michaelgarland579
@michaelgarland579 2 дня назад
Yea that sucks i had same problem yz125 2003 i changed all crank seals an i finally bought lectron carb an its fix it junk ass mukui carbs suck i love lectron carbs an apex head ​@@MrKawie1001
@davidcorder95
@davidcorder95 2 дня назад
Oh heck yeah I loved that bike same age as me
@PaulvanNieuwenhuyzen
@PaulvanNieuwenhuyzen 2 дня назад
I once had a Yamaha 200 2 stroke 2 cylinder, as a boy of 14/15 year old, and at one point you had a mechanism on the ignition system with, when the engine made more rpm, the spark was made earlier by adjusting the moment that the points were opening. The ignition time was changing with more or less RPM. Now did I buy a complete little set and I just put it on, and the engine did run but did not have the higher rpm anymore. Same as with your bike. I also changed the carburetor, the exhaust pipes, and so on. He had more rpm when I made it leaner, but no power on the top.... I sold the thing before I found that. Then I got a Yamaha YZ250 from I think from around 1985, and there I got the same problem when I got trouble with the engine. The top of that Ignition changer was put on exactly the wrong way, so the ignition time didn't change but stayed the same all time. Again bought it in original parts of Yamaha and I think the did the same thing again: assembled it exactly wrong. I took the top of and turned it 180, so the time changed by more RPM and the problem was gone. It is a bit silly explained, but I am dutch and not very well know with the technical terms in English. I think it is about timing...
@RyGriff
@RyGriff День назад
I learn so much every time I watch a video. Thank you for these.
@user-dn5ok5fz1t
@user-dn5ok5fz1t 2 дня назад
Its obvious man first you need to do a leak down test. You plug the exauhst and pump in air through the intake and see if it holds air. If not its crank seals or the base gasket. Next you check to see if the power valve is coaked up with carbon. Do this and you will find the problem.
@michaelesposito6678
@michaelesposito6678 2 дня назад
Or the hole in the case that was repaired with jb weld
@user-dn5ok5fz1t
@user-dn5ok5fz1t 2 дня назад
@@michaelesposito6678 the leak down test will show where the air leak is weather it be the crankcase seals or the jb weld on the crankcase ...A little soapu water will quickly show the air leak if there is one.
@carrothead8462
@carrothead8462 2 дня назад
Power valve 100 percent😊
@poorsob
@poorsob 2 дня назад
I agree!
@raynyhus2026
@raynyhus2026 День назад
It's acting like an old 1964 jeep I had, when coil started to fail. While cold, it ran fine until it warmed up. As soon as the coil heated up, the spark just scattered. Replace the coil, she ran like a dream.
@craigembry7208
@craigembry7208 День назад
I agree with some other posters, check exhaust for an obstruction before a teardown. Never hurts to check it.
@user-fi3fx5my2s
@user-fi3fx5my2s 2 дня назад
Beautiful bike, you really find nice ones...
@michaelgalli8269
@michaelgalli8269 2 дня назад
Man I buddy had one just like that and that thing was a handful but very fast
@robinbrowne5419
@robinbrowne5419 2 дня назад
Bogging. Hmm. I remember bogging on another bike, but I don't remember what was wrong. It is always interesting to go through the process of finding out what is wrong with the bike and fixing it. 🙂👍
@RadioReprised
@RadioReprised День назад
Wide open throttle, 5 kicks....THAT is your compression. Which was slightly low. Check if the midbody gasket is leaking too if it has one.
@debcamp2359
@debcamp2359 2 дня назад
Can't wait to see part 2.
@Dirt_Bike_Dave
@Dirt_Bike_Dave 2 дня назад
Holy crap..Great deal on this bike..even if it has problems..vintage Hondas are hot commodities now .
@Acknockout1
@Acknockout1 2 дня назад
What a beautiful bike.. watch all your videos,well most of them. You have fixed so many bikes. I have learned a lot from u. You have probably been asked this a lot but do you keep most of them after you fix them and also have you came across a 85 Honda 250r ATC. Or one of my other favorites 200x. Keep doing your thing bro . Your videos are what I end my day with. Thank you
@skeptic3332
@skeptic3332 2 дня назад
This looks like a keeper. Sweet bike.
@scottswygert7165
@scottswygert7165 2 дня назад
You got a great deal on that one!!!
@JonRoundtree-mu5gb
@JonRoundtree-mu5gb 2 дня назад
If there were an obstruction in your pipe it would not idle or rev out either. It’s most likely the power valves sticking. Good luck.
@mattsmith7544
@mattsmith7544 День назад
Incorrect
@abpob6052
@abpob6052 2 дня назад
I had Honda of Troy build me a Brian Swink replica 1995 CR250 team bike. Thing was a beautiful. Was identical except that I had Pro Circuit suspension instead of the factor kits. The growl at full throttle in 3rd gear was amazing. The first day I had it i stepped off it on the left side in my garage with shorts on and the footpeg filleted my calf. Super sharp. Learned a lesson there. Took 20 stitches to close it completely up.
@sebastian_park.95
@sebastian_park.95 2 дня назад
I would like to say the powervalve might be gummed up or not opening right. Great Vid!!!
@user-hj5ml8rr8u
@user-hj5ml8rr8u 2 дня назад
a clean machine!...Thanks for the carb class...how about change the crank seal next...
@Chevchild
@Chevchild 2 дня назад
Lot of well thought out comments . Nice job everyone! 😊
@dixoncider7256
@dixoncider7256 2 дня назад
No kidding. Lots of people with great troubleshooting comments.
@nathanbliss6788
@nathanbliss6788 2 дня назад
cdi? sounds like the spark might not be advancing
@dekon70
@dekon70 День назад
You should also check the jet block gasket. If someone was chasing a carb issue and dipped the carb, sometimes the dip eats the jet block gasket.
@Motoxr32
@Motoxr32 2 дня назад
96 cr250 was my favorite bike of all time! Best engine no frame that year!
@rclmxshift
@rclmxshift 2 дня назад
Powervalves?
@poorsob
@poorsob 2 дня назад
Bingo!
@Paul_Gale
@Paul_Gale День назад
Carb tuning is what i need to do and i learned a lot from your videos Thanks for posting
@royhenson3379
@royhenson3379 2 дня назад
Maybe try FMF pipe & silencer.
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