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6.7 Powerstroke Burning MAJOR OIL - MISTAKES WERE MADE 

TopCorey
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2011 f-350 6.7 powerstroke is burning major oil. Check out what happened and let me know if this has ever happened to you!
#powerstroke powerstroke #diesel #ford
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tags:
6.7 powerstroke
6.0
6.4
5.9 cummins
diesel
duramax
turbo
twin turbo
diesel cold start
built diesels

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12 дек 2022

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Комментарии : 118   
@mitchelgehling5428
@mitchelgehling5428 Год назад
Love seeing the videos man, fellow 6.7 guys so love watching content on them. Would love to see a pull with the new trans and some more sound clips and some races on the 17 6.7. Putting in an S370BB this winter
@UZCOexcavationexperience
@UZCOexcavationexperience Год назад
When is the next thing you’re giving anything for a 6.7 away? I am a brand new diesel owner and I have advocated for gas engines since I was old enough to drive. Now I own my very first diesel 6.7 power stroke all of a sudden I want to be a diesel mechanic lol. You guys are fun to watch. I learned so much from you and I really want to say thank you. So next time you do a giveaway for 6.7 power stroke I am crossing my fingers. I am not a mechanic, and this is the third time taking this turbo out and putting in a different one. I can almost do this in my sleep now. I have used some of your videos to help and I want to say thank you again have a great day. Happy new year Cory and the crew!
@TexasTagz
@TexasTagz Год назад
Over pressure probably has to go to vent somewhere. That’s freaking wild.
@kyleduvall
@kyleduvall Год назад
I really enjoy the troubleshooting videos. Good stuff.
@matthewrogers2682
@matthewrogers2682 Год назад
bro i love your channel its super informative on these trucks been watching for a long time and im so glad my 15’ is completely deleted with a BD Scorpion kit i just wish i cld get the vgt sensor code deleted to be able to use my key start again
@elchingon203
@elchingon203 3 месяца назад
I had the same thing I bought new hoses and even air/water intercooler now I wish I had seen this video before my hose was kinked and that fixed it all! Thank you for your video!
@jackiehowton110
@jackiehowton110 Год назад
Not sure if a tone has mentioned it but 6.4 and 6.7 powerstroke have positive crank case pressure so where will always be oil mist from the vent or oil fill
@houstoncartwright3120
@houstoncartwright3120 Год назад
I had the same issue with mine and it ended up being my CCV reroute hose was kinked
@6doorshopdavid980
@6doorshopdavid980 Год назад
He knows the problem he just making videos that ccv was not flowing enough at all
@whiskersmcmeow6224
@whiskersmcmeow6224 Год назад
Bingo
@cappsford
@cappsford 21 день назад
I’m so glad i found this video. I was about to buy a new cac. Then i stumbled onto this video. Fixed my problem as well. Mine runs over the trans and out the passenger side. So i had a kink where it bent across the top. Fixed it, no more white smoke. Just weird it took almost 9000 miles before it started
@trevormangus7832
@trevormangus7832 Год назад
Double check that your CCV reroute is not plugged the part they goes into cover also
@jakethesk8roberts763
@jakethesk8roberts763 Год назад
Great content brother pstroke’s 4 life bud 🍻
@35057
@35057 Год назад
Love your vlog style videos man. Keep it up. Reminds me of fucking off, screwing around back in the day w my buddy.
@James_M_Jay
@James_M_Jay Год назад
You are definitely going to develop some oil leaks with all of that pressure in the crank case
@2alawabidingcitzen
@2alawabidingcitzen 8 месяцев назад
I just post a short of my 02 7.3 smoking it was my CCV blocked after doing the mod. But I put that ish right back when I put my spoologic turbo and up-pipes s&b cold air intake
@ryanbrown918
@ryanbrown918 Год назад
There's something 100% up with your CCV Internal Catch Can/Re Route.
@edwardrichards9181
@edwardrichards9181 Год назад
Oh man, so close hahahaha. Great videos, keep them coming.
@miketerzo3200
@miketerzo3200 Год назад
new viewer here; learning lots with your videos! just curious on the wheel and tire set up on the single cab. not sure if youve talked about it in past videos.
@TexasTagz
@TexasTagz Год назад
How’s the new trans running on the 17? Need some pulls on it🤘🏻
@garylong7096
@garylong7096 Год назад
Good luck, my friend. Had two power strokes, the 2012, exhaust cooler went bad, $10,000.00 repaired. And the 2013, dump truck spun its bearings, at 28,000 miles on motor. Ford wanted $ 25,000.00, to put a new generation 3, installed. Traded both. Do like the new 7.3, pickup. And love the new International CV, dump truck.
@marcuskeim8392
@marcuskeim8392 Год назад
I had the same problem with my work truck..my problem was the ccv was clogged
@Chase-uc1uh
@Chase-uc1uh Год назад
Helping the algorithm 👊🏻
@mark_built
@mark_built Год назад
Why would it also burn coolant as well to though ?
@hoshwilson
@hoshwilson Год назад
My 2012 literate just started doing the same similar thing. I just installed the SPE internal catch can and ccv reroute. I need to check to see if I have the hose kinked now. Great video!
@brad6523
@brad6523 9 месяцев назад
Catch can will always cause higher crank pressure because they all restrict venting the crank
@2alawabidingcitzen
@2alawabidingcitzen 8 месяцев назад
Kc turbo channel have a video about this same thing. That ccv tube gotta be causing to much resistance gotta think the turbo pulls it out.
@tonycloutier8148
@tonycloutier8148 Год назад
Sounds like CCV valve plugged as in the hose or the because it has the SPE kit there should be pleanty of air coming out of that hose
@MT454
@MT454 Год назад
love the trx, hate how a 100K+ truck sounds like it has a valve tick from factory lol.
@chrisstupakPM
@chrisstupakPM Год назад
Same thing happened to me when I deleted my egr with the smoke. Took off the pass through plate under the block plate and it was fine. Weird.
@colt4528
@colt4528 Год назад
Personally I was leaning towards the exhaust bearing went bad!
@marcosolveratxful
@marcosolveratxful 2 месяца назад
Looks like I have the same issue, but my oil level dropped. Makes me think I am burning oil. I don't have any oil leak at all. Any ideas of what my problem could be. I just downloaded Forscan to see if I can find any issues please help. Thanks in advance.
@mjmjersey
@mjmjersey 10 месяцев назад
I'm debating between getting a 6.7 powerstroke diesel or a 6.2 gasser. I'm trying to see if I could get one with 200,000 miles it's probably going to put me in it 16 or 17 is it too risky
@bluntsi7395
@bluntsi7395 6 месяцев назад
Hey so question mines a 2012 160k miles the cap doesn’t blow off when I first take it off but if I push it back in and don’t screw it flys off I can catch it mid air lol that bad?
@beowulf885
@beowulf885 Год назад
pcv valve stuck shut or partially open seems like, your pcv sounded like it was hissing versus normally pushing air
@BadlandsVViLL
@BadlandsVViLL Год назад
Man I hope you guys can figure it out.. I was thinking head gasket but your coolant isn’t boiling
@marcsheppard2898
@marcsheppard2898 Год назад
The turbo pulls crank case pressure out. Put it back the way it was.
@dethrone1300
@dethrone1300 7 месяцев назад
Same I was out ov town working lol judge me but it was a 6.4 power stroke travel 20k on last year for work so...had to get the 6.7 to tow it back 😅
@DiscordCriminal
@DiscordCriminal 9 месяцев назад
I was running an 80hp LBF tune and I found if I hammer it my truck smokes kinda grey any other tune it’s just black. No clue if I should worry or not 🤷‍♂️ I took the LBF tune off because I really don’t want to smoke black or grey. Right now I have a 80hp hiss that doesn’t smoke unless I’m in 5th going 50 and give it 3/4 throttle. Less smoke the less likely to get in trouble
@jordanpavlic383
@jordanpavlic383 Год назад
I’d really like some input if anyone has two cents. I have a 2012 with 200k miles’s, I have a slew of injector codes. I get a CEL for cyl 3 or cyl 5 of contribution/balance they’re never on at the same time it’s either one or the other, I believe it’s causing a fuel knock???… I have white smoke coming out of the exhaust, are two injectors failing??
@sammyholtzclaw7994
@sammyholtzclaw7994 5 месяцев назад
Have you had the cover be kinked and also have oil running down both side of bell housing?
@SeaPro360
@SeaPro360 Год назад
Where did the coolant go?
@mitchbenefield8783
@mitchbenefield8783 Год назад
Kc turbos has a video on their RU-vid channel discussing this exact problem. If I recall correctly it’s bc of the ccv reroute and it being a bad idea. Every time they have this issue they hook the ccv back up properly and issue goes away completely.
@dchilton
@dchilton Год назад
That round blue oval would be the problem with them all since 2003. 7.3 pre-Def for life.
@alsplumbingservicesllc2971
@alsplumbingservicesllc2971 Год назад
Where can I find a good 6.7 motor for 2016 f 250
@user-yx7kb8mt2r
@user-yx7kb8mt2r Год назад
My 6.0 had the same problem!!!
@slorice8723
@slorice8723 Год назад
Thanks for the video. I’m waiting for the SPE intercooler piping, CCV delete and disaster prevention kits to come in for my ‘11 6.7 so good to know if I run into the same issue.
@2230user
@2230user Год назад
Good luck, better off going through a different company if you want it anytime in the near future.
@slorice8723
@slorice8723 Год назад
@@2230user I looked the SPE kit and HSM upper intake. Both were on back order but Im supposed get SPE kit in the next few weeks.
@kylepinder6.7
@kylepinder6.7 Год назад
The spe kit is not one of the good kits on the market. Try the s&s disaster prevention kit. More liked in the community and I run it. I don’t run much spe parts other than a hot side pipe. Spe kinda has a bad rep in the community
@Spsonasty
@Spsonasty Год назад
I got tired of waiting for my ccv reroute and Disaster kit so I went with Smeding Diesel. I’m happy with the result.
@tomparsons3093
@tomparsons3093 Год назад
Check the pcv valve filter
@andrewzonneveld1129
@andrewzonneveld1129 Год назад
Bad valve seal?
@Raider113ci
@Raider113ci Год назад
What’s the point of the CCV opposed to just clamping the hose on the valve cover fitting and letting the blow by hose blow to the ground another words just bypass the CCV??
@TyNeePen15
@TyNeePen15 17 часов назад
When I first started watching the video I originally thought there was an issue with the turbo. But as soon as you removed the oil fill cap and saw all of that pressure and also the smoke went away (that still seems like a lot of blow by imo), I started yelling at the screen "Check the CCV hose!". I wasn't sure if it was pinched or just installed incorrectly.
@TyNeePen15
@TyNeePen15 17 часов назад
Luckily you didn't blow any seals with all of that pressure in the crank case. Hopefully the oil level was checked and topped up if need be.
@ishmelly210
@ishmelly210 Год назад
Tire size and make ?
@blaketerry8569
@blaketerry8569 10 месяцев назад
Mine done the same thing then it started having major blow by out the ccv reroute couple months later. Well a year later I’m dropping a new engine in my truck with 202k miles on it
@tomfarmer6571
@tomfarmer6571 Год назад
Coolant hose collapsing when the truck is not running and is cooling off is normal. I would like to order this kit for my 2012 f350
@tomfarmer6571
@tomfarmer6571 Год назад
I’m excited. Thank you Love your channel
@mjmjersey
@mjmjersey 10 месяцев назад
I noticed you driving a Dodge Ram do you prefer Dodge Ram to Ford Powerstroke 6.7
@stung93
@stung93 Год назад
Had the same issue, mine was ccv.
@montanahall1
@montanahall1 Год назад
My 2015 f-250 is doing the same thing with the white smoke but I don’t have a CCV. The turbo spools fine, truck gets good power, there’s no coolant in the oil, idk what the problem is! Any help would be greatly appreciated
@kevinoneill41
@kevinoneill41 11 месяцев назад
Pluged DPF and EGR is full of gunk and soot they both need the full delete option
@paytonteague2651
@paytonteague2651 8 месяцев назад
Mines the same way I have stock ccv and white smoke very small amount and it’s coming out of the exhaust
@paytonteague2651
@paytonteague2651 8 месяцев назад
Did you ever figure out problem
@benklesner2566
@benklesner2566 3 месяца назад
?
@JavierMedel-co3in
@JavierMedel-co3in 3 месяца назад
@@paytonteague2651I was told today that my dually needs the updated ccv box since the one it has is defective, sounds to me like a recall but they said it’s not
@joshgenrich3234
@joshgenrich3234 Год назад
Why does that upper rad hose pancake ? Mine did that after I flushed coolant maybe cause it needed to be topped off not sure
@marcosolveratxful
@marcosolveratxful 2 месяца назад
Same thing happened to me, I filled the secondary reservoir tank and fixed the problem.
@Motoxkid34
@Motoxkid34 Год назад
I have a 2016 6.7 powerstroke ,tuned and deleted, when I get on it every thing is fine but when I let off the throttle I get nothing but white smoke . Can you help me out … i also had a muffler flo pro muffler on and switched it out to 5” straight pipe , then started having issues
@johnsparks7593
@johnsparks7593 Год назад
Having the same issue, lmk if anyone figured it out.
@johnsparks7593
@johnsparks7593 Год назад
I took the cap off and it fixed the issue, which means ccv.
@ryansnow2598
@ryansnow2598 Год назад
Pretty crazy to see the Ikea right by my work on RU-vid
@pickeltop_1769
@pickeltop_1769 Год назад
and i thought you were selling this corey XD
@marioquiroz5114
@marioquiroz5114 Год назад
What exhaust tip is that??
@TopCorey
@TopCorey Год назад
THE BIG ONE
@Honeybadger-wg5fi
@Honeybadger-wg5fi Год назад
My truck was doin exactly same thing after I put upgraded cold side intercooler pipe started smoking like a freight train and was loosing coolant but there wasn’t any in oil and no leaks put some stop leak in it and coolant stopped disappearing and would only barely smoke shop told me was turbo goin bad mines 2012 f250 6.7
@mattwnovak
@mattwnovak Год назад
Put a spring in the ccv house so it doesn’t kink
@fredvincent4224
@fredvincent4224 3 месяца назад
this is the best color on a 250 I have the same
@calebcochran5133
@calebcochran5133 4 месяца назад
That’s a pretty ford
@chrismarichalar7919
@chrismarichalar7919 Год назад
ccv re routes are the problem go watch kc turbo video on this its like a year or two old already
@cap6859
@cap6859 Год назад
Absolutely agree. This is why I’ll never do it to mine
@tonycloutier8148
@tonycloutier8148 Год назад
Works fine u have to get install it properly
@tonycloutier8148
@tonycloutier8148 Год назад
If u ever want to sell the dual intake SPE pipe that goes to the S&B let me know Dan want sell it separately
@NickySull
@NickySull Год назад
check ccv reroute for shore
@justinfannon8159
@justinfannon8159 Год назад
hmm i just bought this re-rout kit, now im not sure
@TopCorey
@TopCorey Год назад
user error
@TheRockinProduction
@TheRockinProduction Год назад
Positive Crankcase Pressure from the CCV Reroute caused the turbo seals to blow sir. CCV Reroute is a bad idea. Put the stock CCV box back on, problem solved.
@TopCorey
@TopCorey Год назад
unkink the hose, problem also solved
@shearenergy8203
@shearenergy8203 Год назад
I check for kinks,twist,pinches,and stoppages everyday by using my guy in my pockets however may need realignment more times than often
@rauldelgado2621
@rauldelgado2621 День назад
Ccv filter, oil separator
@danielhull279
@danielhull279 Год назад
The upper radiator hose sucking shut like that is completely normal condition. Fords have been doing that for years gas and diesel alike.
@tannersmith8889
@tannersmith8889 Год назад
ccv reroute and a new turbo is needed
@2alawabidingcitzen
@2alawabidingcitzen 8 месяцев назад
It was the fact of having that long tube on there was just enough resistance.
@nathanneuherz4144
@nathanneuherz4144 6 месяцев назад
I would have named the video 6.7 Powerstroke Oil Fill Cap Delete (Must need modification)
@BG-xh5rb
@BG-xh5rb 8 месяцев назад
Leave the stock CCV intact. Change/service within standard intervals.
@ifronnin
@ifronnin Год назад
I'm commenting before the video ends, but sometimes DEF diluting the fuel will force oil out the tailpipe. It looks exactly like a blown turbo seal.
@glennblum6410
@glennblum6410 Год назад
PVC clogged
@Kodi5204
@Kodi5204 Год назад
Running it like that isn’t smart that’s a quick way to make every seal suck in and leak
@davecampbell1452
@davecampbell1452 Год назад
Ford hat driving a dodge
@soggywaterz2064
@soggywaterz2064 Год назад
I’m early
@lyndonhamby7432
@lyndonhamby7432 Год назад
What did you expect. It’s a ford brother 😂
@asherflesch7423
@asherflesch7423 Год назад
Had my cp4 let go on me and caused an injector to stick and it washed cylinder 5. My intercooler was blown, and truck was already lower on compression. New longblock and updated fuel system with my s467 turbo should be a hell of a lot better than 67mm on low compression and hurt fuel system.😂😂
@jakethesk8roberts763
@jakethesk8roberts763 Год назад
How many miles you have on it and what year 6.7 did your cp4 go out in do u use fuel additive every fill up ?
@justinweaver6860
@justinweaver6860 Год назад
Seems like someone needed something to make a video. Like come on....thats very obvious what the issue was as soon as he started checking it!
@davidcarder6364
@davidcarder6364 Год назад
Yep,junk.
@russellaustin4988
@russellaustin4988 Год назад
CCV reroute are junk.
@RamandChevyOwner
@RamandChevyOwner Год назад
Typical ford
@treesquatch9150
@treesquatch9150 Год назад
Too many commercial breaks, I'm out
@tonyxenos1818
@tonyxenos1818 10 месяцев назад
I spent $20,000 tryin to fix this damn problem. Head gasket, studs, new turbo, Intercooler, nothing fixed it. Sold truck cuz of it at huggeeeee loss. Didn’t wanna screw next guy. It never got fixed though
@JoseHernandez-bl9en
@JoseHernandez-bl9en Год назад
Dont drive it no more if you can’t deal with the issues perro
@yosimitesam67
@yosimitesam67 Год назад
Powerstrokes are junk.
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