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Laser Cut Parts for the hobby shop! 2kw Laser 4 in 1 Welder & Cutter machine cutting parts! Part 1 

K-Rigg it!
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Do it yourself way of building and installing a 4 in 1 2000w (2kw) Fiber diode laser, welder and cleaner on a CNC Plasma Table. Metal Fabrication to the next level!
/ @kwrigg
0:00 Intro
2:15 Laser Welder Overview
9:05 Bracket Fab
10:38 Wiring
13:30 Fiber Laser Cutting

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24 июл 2024

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Комментарии : 5   
@TimWelds
@TimWelds 26 дней назад
That’s an awesome integration, nice work!
@trebronikum
@trebronikum 25 дней назад
Nice man. I also thought of this. Bought a 2kW 4 in1 laser a month ago, will do the same conversion. My only concern is i think these welder heads won't tolerate well if the laser reflects back itself.
@kwrigg
@kwrigg 25 дней назад
Thought of the reflection being an issue too but I make sure I’m not pausing on the pierce and have the machine moving instantly to keep the laser beam from reflecting back. Just make sure the lead in is long enough to let the laser get all the way through before you get to the profile lines.
@celiougo
@celiougo 23 дня назад
Muito bom... Como vc fez para diminuir o delay. Tenho uma hand laser de 1500w, mas tem um delay de 1.2 segundos entre apertar o gatilho e abrir o laser... e as vezes dá uma pequena variação nesse tempo... +- 0.5sec Vou cortar chapas de aço inox de 1.2mm. Sobre a pressão do ar comprimido... abaixo de 100psi cria muita escória na borda. Obrigado. Penso em usar O2 puro.
@kwrigg
@kwrigg 13 дней назад
English Translation: "Very good... How did you do to reduce the delay? I have a 1500w hand laser, but there is a 1.2 second delay between pressing the trigger and opening the laser... and sometimes there is a small variation in this time... +- 0.5sec I will cut 1.2mm stainless steel sheets. About compressed air pressure... below 100psi creates a lot of slag on the edge. Thanks. I'm thinking about using pure O2." On the Laser unit control screen, there is a setting for delay of cutting from flow of gas to start of laser. I didn't mess with it and just made sure my lead in was long enough. If you have variation in start time, it might be in the safety clamp not getting a good connection between your cut piece and gun. I'm running right around 100 psi but might be dropping under 100 psi while the laser is cutting so my next step is upping the psi. Im planing on using oxygen when i try cutting thick steel as I have read this will increase the thickness available to cut.
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