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Mini Lathe Reverse Gear Noise Problem Fix - Part 1 

Richard Moore - Engineering at Home
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When I put my mini lathe into reverse it caused the gears for the power feed to grind horribly. In this video I take you with me on a journey to diagnose what the problem is and to work out how to fix it.
We're going to be stripping down the gearbox, rebuilding it, making some new parts for the lathe and even make some tools to help us along the way.
The fix applies to the following lathe models: CJ0618, Crenex 7"x14", Clarke CL300M, Warco Mini lathe, Sieg C2 and many other brands which are based off the Chinese mini lathe design.
Watch Part 2 Here - • Mini Lathe Reverse Gea...

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27 фев 2023

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Комментарии : 36   
@paulhelman2376
@paulhelman2376 День назад
Very nice approach which rings true to me. I admire the orderly quality of your work shop
@radboogie
@radboogie 6 часов назад
Thank you very much!
@paulhelman2376
@paulhelman2376 День назад
a simpler depth Guage would be a rod within a tube that has a long slot cut in and marked with a measurement scale. A mark on the rod would show the depth it has moved in the tube.
@BedsitBob
@BedsitBob Месяц назад
When grinding HSS tool bits, there's no need to worry about overheating them. They'll be far too hot for you to hold, long before you affect the hardness.
@paulhelman2376
@paulhelman2376 День назад
looks like you removed the plastic guard shield?
@radboogie
@radboogie 9 месяцев назад
If you believe this channel deserves a subscription, this is a thank you in advance.
@SgtCude59
@SgtCude59 Год назад
Very interesting video. I’m going to see if what your doing will fixes mine
@radboogie
@radboogie Год назад
Thanks mate, hoping to re-machine the tumbler gear detent shaft in the next few days which will hopefully sort it for good.
@radboogie
@radboogie Год назад
I should have mentioned, in part 2 I machined a new bush for the tumbler gear lever pivot, this reduced the reverse gear noise quite a bit. ru-vid.com/video/%D0%B2%D0%B8%D0%B4%D0%B5%D0%BE-j4vh6xuiS0s.html
@jenniferrobinson4277
@jenniferrobinson4277 3 месяца назад
When you're cooling your tool, I kept wincing as you crossed the face of the grinder with your right arm. Get some wire and hang a mug of water off the front of the grinder. Quicker to reach and no amputations.
@radboogie
@radboogie 3 месяца назад
The camera angle made it look worse than it was, there was no danger.
@incubatork
@incubatork Год назад
watching the lever at the back it lfts slightly and the noise starts, try putting some weight on the lever to see if it helps by stopping it lifting.
@courier11sec
@courier11sec 10 месяцев назад
Thank you for the informative video. I wonder if your video editing software allows you to attenuate the sound a bit while machining?
@radboogie
@radboogie 10 месяцев назад
Thanks for the feedback, will see what I can do for the future videos.
@courier11sec
@courier11sec 10 месяцев назад
@@radboogie so I went on to watch your next few videos on this project and the way you are attenuating the machine sound and adding music is perfect. Thank you for sharing your project. 🙂
@radboogie
@radboogie 10 месяцев назад
@@courier11sec thanks, we're evolving as we go 👍
@timmontano8792
@timmontano8792 6 месяцев назад
I think I would have just drilled and tapped some grub-screw holes in the little tubular protrusion that holds the lever in the forward and reverse positions. This way I could simply screw those grub-screws in or out the correct amount to mitigate or stop all together the upward movement or backlash of the forward and reverse handle. It might be tricky to drill at that particular angle but considering that you went through all that trouble with the first attempt to fix this, I think it might be worth your while.
@radboogie
@radboogie 6 месяцев назад
Thanks for sharing your ideas Tim. I was really happy with the final fix at the end of part 4, and happy that some of the steel on aluminium bearing surfaces are now protected by brass bushes. But there are definitely quicker and easier ways to achieve a workable end result.
@SgtCude59
@SgtCude59 Год назад
Saw something very interesting to me . Where you get your indicator you have on your lathe
@radboogie
@radboogie Год назад
I made it from a digital Tyre Tread Depth Gauge. I cut it down a bit, made a brass slider to go under the scale which I could spring load, and 3D printed a housing for it. Here's a link to a similar one on eBay - ebay.us/36ZOND
@MartyGIJoe
@MartyGIJoe Год назад
@@radboogie you have video of making it
@radboogie
@radboogie Год назад
I don't have a video on making the "Tyre Gauge DRO" but will do one when I have time. Can upload the drawings and 3D files to the RadBoogie website if you would like to make one yourself.
@Pusolandia
@Pusolandia 8 месяцев назад
Hi and compliment for the video, very interesting. I have this lathe and I would to buy a tailstock with chuck to make holes, can you advise me of a link where to get it? thanks and ciao from Italy
@radboogie
@radboogie 8 месяцев назад
Thank you. The mini lathe I have is the same as the Clarke CL300M, Amadeal of London do a tailstock for mini lathes that is compatible with the Clarke CL300M so you could look at that. I bought a Clarke CL300M fixed steady and that fitted my lathe perfectly. Amadeal say the centre height is 90mm, I just measured my lathe and the centre height is correct at 90mm. I would recommend asking them for some dimensions of the dovetail to make sure it will fit, to be sure. www.amadeal.co.uk/cgi-bin/sh000001.pl?WD=tailstock&PN=Mini%2dLathe%2dTailstock%2dwith%2dTailstock%2dLever%2dLock%2dAMA_SP_CJ18_138RB%2ehtml#SID=14
@1crazypj
@1crazypj Год назад
Wind the compound/top slide back so it's supported instead of overhanging, things wont move around as much. (a QCTP moves tool further away from clamp point plus the extra 3/4"/19mm wound forward?) It sounds terrible, maybe you should have just left the gear train off and hand feed saddle/carriage like you did when boring? The belt drive works fine without the gear train (may be worth checking the belt sits properly as well, on some mini lathes the gears don't match belt teeth pitch. 'Plan C', make a complete new reverse tumbler Cool idea with tread depth gauge.
@radboogie
@radboogie Год назад
Yes, I usually put the lathe in neutral when not power feeding to quieten it down. In part 4 I drill an extra hole in the gearbox for the detent which makes it easier to put the thing in neutral and bypass the gearbox. I'm going to work on quieting the lathe down in future videos, will make an interesting project. Thanks.
@reaper42469
@reaper42469 Год назад
That handle should tighten up if you twist the knurled part of the handle at least mine does
@radboogie
@radboogie Год назад
Thanks Reaper. I tried what you suggested but it didn't fix the problem for me. Hopefully that can help someone else who has the problem - cheers for sharing.
@johnhall1018
@johnhall1018 Год назад
I couldn't be living with the spindle bearing whine! Do you think they bothered to grease them at the factory?
@radboogie
@radboogie Год назад
It sounds worse on the video, mostly it's electrical whine from the motor drive circuits. I filter out the whine on later videos to be easier on your ear.
@johnhall1018
@johnhall1018 Год назад
Much appreciated, i enjoyed the videos, with the sound off. 😂😂
@radboogie
@radboogie Год назад
@@johnhall1018 😂
@winandd8649
@winandd8649 7 месяцев назад
These chinese lathes can be horrible 😵‍💫. I'm glad I made the choice to buy a second hand Emco (very pleased with that)
@radboogie
@radboogie 7 месяцев назад
True. You buy a Chinese mini lathe and use it to repair your Chinese mini lathe.
@winandd8649
@winandd8649 7 месяцев назад
@@radboogie Yeah, it's a hobby in itself😆
@buddysmith7462
@buddysmith7462 Год назад
that's your reverse gear lever pull it down to go in reverse
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