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More Improvements to the Harbor Freight 20 Ton Hydraulic Press Part 2 

Dudley Toolwright
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This video includes further improvements to the Harbor Freight 20 Ton Hydraulic Press.
Please Note: I am a beginning machinist and I do not pretend to know everything. Please always operate machinery in a safe manner and if you don't know, find a reliable source. DO NOT COPY ME. I make a lot of mistakes. I provide these videos for entertainment only.

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26 авг 2024

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Комментарии : 582   
@oldschoolways4661
@oldschoolways4661 5 лет назад
Taking the extra time to not just come up with a solution but making it ascetically pleasing. Nice job. I have a lot of tools but no lathe. Now I'm wishing for one.
@DudleyToolwright
@DudleyToolwright 5 лет назад
Every tool I get opens new possibilities. I really do sympathize with the addiction. I hope you find one soon. Cheers.
@Gkuljian
@Gkuljian 6 лет назад
I've watched every video on bottle jacks, and this is the first that actually shows the details of how they're put together. Thank you for that. It's easy to sit on this side of the video, and comment. But I seriously doubt the lifting shaft could tolerate the forces if it were cast iron. It's great to know how that thing is made. My press consists of a bottle jack and a very big section of I-beam. One of these days I've got to put a press together. These videos have provided some great ideas.
@DudleyToolwright
@DudleyToolwright 6 лет назад
I never mind comments, they always provide food for thought regardless, so don't stop. I think you are correct about the strength issues with cast iron. What got me thinking in that direction was the bottom press in piece, which looked like cast iron and was. At the time I thought the whole assembly was a single piece of material. In hindsight, I probably should have known better. I was expecting some sort of case or through hardened shaft, but what I found was, at least to my ignorant self, surprising. Thanks for keeping me thinking.
@paulng5768
@paulng5768 6 лет назад
You might be able to figure out if the piston is hollow or not by weighting it.
@28cruzin
@28cruzin 6 лет назад
Nice job! Clever use of the extra ram. Most times I've seen slip on adaptors for different apps of the standard bar. You still may use them, but having that screw in the old ram is priceless. Again, Nice Job!
@DudleyToolwright
@DudleyToolwright 6 лет назад
Very kind, thanks.
@elfinyootube7971
@elfinyootube7971 5 лет назад
I like the way you do these videos, for a hobbyist, you do real nice work. Everything you say is to the point and informative. no wasted words, unlike a lot of guys who really must love the sound of their own voice...
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks. I try to edit out everything bu the essentials. Sometimes I get it right.
@02arleigh
@02arleigh 5 лет назад
I like your innovation , I have a similar press I've modified as well . Some folk do not understand why go to all this, but something is learned every time you think out of the box , and oft times it's far better than want is currently available . My innovation is providing the capacity to open 2 ways ,rather than having only one .
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks. I agree completely. It was fun and a learning experience, especially since I have gotten a ton of constructive feedback from the community. I appreciate it all.
@ColdWarVet607
@ColdWarVet607 5 лет назад
Every time you makes an improvement, please send me the piece, I should have a full press in about 10 more episodes? Fantastic Loved it...whens Part 3?
@DudleyToolwright
@DudleyToolwright 5 лет назад
I have some ideas...thanks for the encouragement. I appreciate the feedback.
@bobblack3870
@bobblack3870 5 лет назад
I like all of your ideas. I bought 20T HF press a few years ago that came in orange. I like your color much more. The number one thing that bothered me was those two black springs that lift everything back in place when finished. I think the main issue was mine were not tightened enough and stretched with time, so I was always practicing arm curls to get the unit back up. Finally, I replaced them with a cable and weight system. I should make a video of it, but here is what I did: I used 3 OH garage door cable pulleys (3") on each side. That style of pulleys have ball bearings. For each side: I ran thin steel cable from the top horizontals (drilling and inserting a bolt between them to attach the cable end), down to a pulley on the "press bar", then straight back up to a 2nd pulley above the top horizontals. The cable stays between the two top horizontals. There is a 3rd pulley cantilevered to the side of the press. Two wide sheet-metal "angle irons" sit above and are bolted to the top horizontals, sandwiching pulleys 2 & 3 for their support. So the cable path goes down, up, horizontal, then finally hangs down to a suspended weight. My weights are scrap iron, each weighing 20 lbs which is overkill because of the multiplication factor with the press bar pulley. It all works very smooth and always pulls the bottle jack up tight.
@DudleyToolwright
@DudleyToolwright 5 лет назад
Neat solution. No matter what I come up with and no matter how long I have thought about a problem, someone else always seems to come up with a unique solution I had not thought of. Very nice and thanks for sharing.
@rancher9625
@rancher9625 5 лет назад
@@DudleyToolwright If video makes this easier to understand, search for 'Harbor Freight Shop Press Pulley', (ru-vid.com/video/%D0%B2%D0%B8%D0%B4%D0%B5%D0%BE-3y3MQRTYtY0.html). It is an unpolished quickie video.
@tkskagen
@tkskagen Год назад
Fabrication and Modifications are "KING" to make the Tool you need!
@DudleyToolwright
@DudleyToolwright Год назад
Thanks and let's not forget fun.
@matthewwhaley1605
@matthewwhaley1605 3 года назад
Man I never comment on any videos. But i read a lot of comments. It's awesome you take the time to reply to comments. And receive constructive criticism openly. Keep being rad!
@DudleyToolwright
@DudleyToolwright 3 года назад
Thank you very much. I figure that if the community is willing to spend their time to offer advise and comments, it's the least I can do to respond.
@tobyw9573
@tobyw9573 5 лет назад
Some people clamp their chuck on a shaft/broomstick to provide a good handle. I have also seen wood blocks with side stops like wheel chocks to prevent rolling. Rolling the chuck off onto your foot is a BIG consideration along with denting the ways. Thanks for sharing!
@DudleyToolwright
@DudleyToolwright 5 лет назад
Good suggestions, thanks. I usually set the chuck onto the d-pins when I am not holding it, but man I can imagine my 4 jaw hitting a toe...what toe?
@bulletproofpepper2
@bulletproofpepper2 5 лет назад
I had a project i needed to crimp the ends of pipe. I think it was 125 pipes crimped both ends. I turn on the air motor full time and just opened and close valve. It worked well. Thanks for sharing
@DudleyToolwright
@DudleyToolwright 5 лет назад
I would love to see a video on that one. Thanks for sharing.
@JayFude
@JayFude 2 года назад
You had me at "Release the Schmoo!" and subscribed!
@DudleyToolwright
@DudleyToolwright 2 года назад
Thanks. I did steal that comment from aVe. His play on words always amuses.
@dennisgeroux4483
@dennisgeroux4483 Год назад
Nice additions, you gave me some ideas on modifications to mine.
@DudleyToolwright
@DudleyToolwright Год назад
Glad I could help
@petedetects7012
@petedetects7012 2 года назад
Very good improvement, I own the orange version of that jack . So many times I feel I can improve it but fight the little time I have in my shop to do anything about it. Thanks for sharing
@DudleyToolwright
@DudleyToolwright 2 года назад
Thanks. It was fun trying to conceive of ideas to improve a really mediocre, but affordable press.
@trollforge
@trollforge Год назад
Nice job Robert, the use of the second Ram is simply genius!
@DudleyToolwright
@DudleyToolwright Год назад
Thanks. I have limited room to store things, so that was a partial motivating factor.
@trollforge
@trollforge Год назад
@@DudleyToolwright If you look at some of my older fabrication videos, you'll see that my shop is half again, if not twice the size of yours, with about 1/4 the space... ;)
@jamesdorsey1686
@jamesdorsey1686 4 года назад
Great shop walk through, I also believe in constant shop upgrades. Your ideas work Dudley. The only problem I had was time, now I have to quit my job to catch up.
@DudleyToolwright
@DudleyToolwright 4 года назад
I feel ya. There is never enough time to get even a tiny percentage of the projects done. I have a full time job as well.
@DereksWorkshopAndProjects
@DereksWorkshopAndProjects 5 лет назад
Your down right impressive for a hobby guy. I suppose the biggest thing is having the right tools but everything your doing seems really quite well done. Great job!
@DudleyToolwright
@DudleyToolwright 5 лет назад
You are very generous. Thanks for the kudos.
@thepubliceye
@thepubliceye Год назад
I'm not impressed, the guy has a lathe he should have made that piece.
@loloforge2841
@loloforge2841 3 года назад
Dude! The title of this is “Make Improvements to the Harbor Freight 20 Ton Press...”, you should have taken a few more episodes and call it: “How to make your own USA made 20 Ton Press with dual adjustable pistons”!!! Lol. Solid work man, solid!
@DudleyToolwright
@DudleyToolwright 3 года назад
Thanks. In case you missed them, there were also a couple of other videos with improvements and one where I looked at how much force the press could actually produce. Happy New Year.
@themotofixery
@themotofixery 4 года назад
This is such great stuff! I've been waiting for this press to go on sale and tomorrow is the day so I'll be using some of your great ideas. I really appreciate all of your videos and can't wait to get to work on this project. Thanks!
@DudleyToolwright
@DudleyToolwright 4 года назад
Hope you enjoy it!
@Kevin_747
@Kevin_747 5 лет назад
Good useful mods. My HF 20 ton press came with the round stock welded in crooked and I didn't unbox it till well after the 90 day warranty. So I need to make a straight ram.
@DudleyToolwright
@DudleyToolwright 5 лет назад
I do consider purchases at Harbor Freight to be a bit of a coin toss. Sometimes you really do win though.
@mohabatkhanmalak1161
@mohabatkhanmalak1161 4 года назад
There's plenty of room for improvement on these Chinese, Taiwanese made equipment. They tend to use cheap, re-cycled steel which are softer and full of other elements. We are seeing a trend towards these kinds of re-engineering lately and this clip is one of the best. My 1950's British made press is mechanical and I will be converting to hydraulic soon. Thanks for posting, enjoyed watching.
@DudleyToolwright
@DudleyToolwright 4 года назад
Thank you for the kind words. I appreciate all comments, but I must say that favorable reviews or people commenting that I helped in some small way are my favorite. If you end up making a video of your update project, let me know. I would love to watch.
@jamesharless5357
@jamesharless5357 7 месяцев назад
Very nice work, and great video!👍🏻
@DudleyToolwright
@DudleyToolwright 7 месяцев назад
Thank you very much!
@thenet0120002
@thenet0120002 6 лет назад
I built my press and i added the ability to thread a large thread into the bottom with a design like the one you showed in the beginning to so i did not have to destroy a jack to have this adjustable feature. I can mount different pushing shapes just by screwing the next attachment in.. I also added a means to raise and lower the press support by adding a houst and cable so i don't have to play with the support which weighs then try to load the height pins .
@DudleyToolwright
@DudleyToolwright 6 лет назад
Very nice. I considered making the threaded portion myself, but I already had the spare jack and I was not sure if I could pull of ACME threads, especially the internal ones, easily.
@thenet0120002
@thenet0120002 6 лет назад
I believe you can buy a acme tap / die to make the threads or you can bore out the center of you punch and braze or weld a thread that you buy into the hole. They sell big nut and threads that could be used . Just suggestion!
@consaka1
@consaka1 6 лет назад
AVE is cool and very informative and his sign off at the end of his videos drives my wife nuts. lol
@DudleyToolwright
@DudleyToolwright 6 лет назад
He is quite entertaining and as his viewership increases he gets nuttier. Put a what, where?
@marscruz
@marscruz 6 лет назад
His sign-off is an homage to The Red Green Show, a Canadian TV program that ended up on the Canadian version of BBC, the CBC. Red Green, the host and main character, would always end the program by saying: "Keep your stick on the ice". A hockey reference that a hippie dude might translate as: "Peace out, bro".
@tobyw9573
@tobyw9573 5 лет назад
I bought a really big pipe wrench to rebuild my floor jack. If I had to do it again I might try a strap wrench made to take a tee handle. ABOM repairs hydraulic cylinders it looks like you need an in at a hydraulics store to get the good prices. Ah, you mention Abom. I agree with dismounting lathe chucks onto a board and have seen some nice custom ones that prevent rolling and position the chuck near its final height. I like the idea of clamping a bar in the chuck as a handle to move and position it.
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks for the comments. I like the strap wrench idea. I only have a small one.
@joedejesus6363
@joedejesus6363 6 лет назад
Great video, I learned something just by watching your channel. Thanks for the "Tutorial"
@DudleyToolwright
@DudleyToolwright 6 лет назад
Thank you, I try, but remember, I am not an expert and if you see something questionable, don't hesitate to call me on it. I always learn a lot from the comments, good or bad.
@davefeinglass9118
@davefeinglass9118 3 года назад
I love how you use tools, to make things for your tools, so that you don't have to use other tools to adjust your tools. (thinking about the knobs for the springs there :). Really great videos, thanks for posting them.
@DudleyToolwright
@DudleyToolwright 3 года назад
Thanks. I'll try not to be a tool and respond using this electronic tool. Wonderful play on words.
@tkskagen
@tkskagen Год назад
When it comes to using your Lathe, I would recommend running down the external diameter to keep "the wobble" TRUE for your application! Sure wish that I had a Sturdy Lathe for the 3× a year (maximum possibility of use) within my shop/garage...
@DudleyToolwright
@DudleyToolwright Год назад
Thanks for the tip. I get the love of tools. Every one opens new possibilities for things you can achieve.
@russelllaferrera892
@russelllaferrera892 5 лет назад
I added a winch with cables crossing over the top of the Press connecting to the handles on each side. I used a bearing w/long bolt across the top of the Press (this is used as cable guides.) The purpose of this set up is to raise/lower the table. This makes it easier when you have a heavy item on the table.
@DudleyToolwright
@DudleyToolwright 5 лет назад
That is a good idea. moving the table up and down is a pain.
@ricklp7938
@ricklp7938 5 лет назад
On my press the channels that form the work table were tall enough to cover a set of pin holes in the uprights . I drilled two holes to accommodate an extra set of pins so it is supported at four points rather than just two . An older press I have has deformed holes in the uprights due to repeated heavy use .
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks for sharing your experiences with this press and possible solutions to the eventual problems.
@wintercoder6687
@wintercoder6687 3 года назад
Wow... I just picked up a HF 20T Press for $154 (on sale). Thought I got a pretty good deal. After watching a couple of these "HF Press Mod" videos, I'm excited to know that If I save my pennies (~$200K worth of them) I too could have all of machines necessary to turn my $159 shop press into a $1K shop press all by myself!! Great video BTW.
@DudleyToolwright
@DudleyToolwright 3 года назад
I get the equipment thing, but others have found way around have large machines. I am sure you could too. The press is a decent deal for the money. Thanks for taking the time to comment.
@riverwizard22
@riverwizard22 6 лет назад
Nice put a triangular gusset on the top piece so as to stabilize it preventing twisting. Above the Jack, Like a 3/16" flat stock on both front and rear, triangular, Like 8"wide on bottom and 12"wide at top or bigger. Nice job . You have machinery I'd love to have... I also have the 20 Ton HF PRESS...
@DudleyToolwright
@DudleyToolwright 6 лет назад
Thanks for the really interesting idea. I have not used this press enough to see the twisting issues. I appreciate the heads up on a solution, even before I run in to the problem. Much appreciated.
@andyZ3500s
@andyZ3500s 4 года назад
I basically have the same press it's just older. It has always done what I needed it to do. I always wanted something nicer but with the modifications that you showed this seems like the route that I'll take. That way I could put the money into something that would expand my capabilities. I'm a new subscriber and enjoy your channel.
@DudleyToolwright
@DudleyToolwright 4 года назад
Thanks, I really appreciate hearing about other peoples perspectives. Thanks for subscribing.
@joegarage6132
@joegarage6132 5 лет назад
First time watching your videos, enjoyed the lathe work. I have the parts for an older press, this gets me some things to think about. I've been welding for over 30 years, you are doing fine. The biggest thing is every time you weld you get better. Thank you for the great work. Btw my daughter set me up to subscribe and I will in a second. thanks
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks for the sub and the words of encouragement. I have a long way to go before I make decent tig welds. I am completely self taught from books and vids. Every once in a while I get a straight clean bead, but that would be the exception. Thanks for the kind words though. I really appreciate you taking the time to share your thoughts.
@joegarage6132
@joegarage6132 5 лет назад
​@@DudleyToolwright Remember keep your metal clean, never use anything other than acetone to clean the metal, Fosgene (sp) gas is a real threat to the welder, look it up. the other thing take your time with your puddles, keep your tip sharp or rounded depending how you like it. Leave your gun tip in the weld until all gas has left at the end of your bead. and remember to breath while you weld. Self taught is not a bad thing, shows desire. Get a scrap piece of metal and practice making your welds. You will get it .
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks for the tips and the encouragement. By the way, for unknown reasons YouTunbe's spam filter keeps moving your posts to the spam folder which is why I missed it when you posted it. Very strange. Thanks again.
@joegarage6132
@joegarage6132 5 лет назад
@@DudleyToolwright well my downfall is computers, I got something on my apple computer yesterday, thought they fixed it, oh well , hope this works thanks for the information
@damirdze
@damirdze 3 года назад
@@joegarage6132 why to bread while welding ? I am not a professional welder too, and I hold my breath to save the lungs and heart from inhaling the gasses or even dust from the process.
@glenglene8473
@glenglene8473 2 года назад
Great contents. You turned $200 press into $2,000 press.
@DudleyToolwright
@DudleyToolwright 2 года назад
Thanks. I am still using the press and it works reasonably well.
@hu5116
@hu5116 Год назад
Nice vid, thanks! On the piston shaft, I’m not sure why you thought it would be cast iron, as cast iron brittle and could shatter under the imperfectly unbalanced loads in a job which was not set up perfectly (most of them ;-). It needs to be incompressible and resistant to bending, while not fracturing.. so it needs tough and strong. Cast iron is hard (so it make a good end cap) but could shatter when bent. IMHO of course .
@DudleyToolwright
@DudleyToolwright Год назад
You make some excellent points. I was factoring in the fact that these tools were sold by Harbor Freight, who used to sell theses presses with cast iron press plates. There are a surprising number of comments talking about catastrophic failures.
@snoopu2601
@snoopu2601 2 года назад
We have a huge drill press looks like it was made in the 1930s has that art deco style to it, we need a motor for it to get it going. We have many industrial tool's heavy duty machine's that we got from old timers that are no longer needing then. They see my brother's and I are always building are working on stuff. I guess they feel like there tool's are going to a good home that will get used. I have many nephew's and there friend's that like building thing's to.
@DudleyToolwright
@DudleyToolwright 2 года назад
The old machines are made to last. With a little bit of effort they can last multiple lifetimes.
@quadpit
@quadpit 4 года назад
I love overkill stuff... Just wish I had your skill set. Great video!
@DudleyToolwright
@DudleyToolwright 4 года назад
You are very kind. Thanks.
@dondotson4604
@dondotson4604 5 лет назад
Thanks Dudley. I'm going to direct copy you. All good stuff.Don from Oregon
@DudleyToolwright
@DudleyToolwright 5 лет назад
That is very flattering, thanks.
@g.tucker8682
@g.tucker8682 Год назад
Btw, ATF can also work well as a cold weather hydraulic fluid. Great ideas here, some I will definitely borrow. Thanks!
@DudleyToolwright
@DudleyToolwright Год назад
That is good to know and it makes sense. Thanks!
@craigwiess1656
@craigwiess1656 Год назад
My old skid steer calls for type F atf instead if hydraulic fluid late 70s early 80s takes a few minutes to warm everything up when it's cold out.
@amrosla67
@amrosla67 5 лет назад
Simply amazing watching you mill your own parts!!! I am just facilitated with any videos on lathes!!! I sincerely appreciate both of these improvement videos and wish you all the best!!! Perhaps you should try and design some type of new Gatling gun that can fire billions of rounds out in a minute for our military!!! Lol Thanks again Art PS: I only got nervous twice in this video and that’s when you’re reaching into the lathe to catch your parts!!! Please be careful as the “Big Guy” upstairs only gave us 10 fingers!!!
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks for the comments and warnings. I appreciate you looking out.
@Z71Ranger
@Z71Ranger 6 лет назад
Great Video... I think if I had your Tools and Knowledge I would have just built the press my self... You do Nice work...
@DudleyToolwright
@DudleyToolwright 6 лет назад
I considered it, but the materials would have been more than the whole press (if I had purchased them from my local supplier). Besides, I was curious to see if I could take a very affordable unit and make it something like the more expensive brands. Thanks for your thoughts.
@173staggerlee1
@173staggerlee1 5 лет назад
or maybe i could do it with my B&D 3/8 drill........seriously, great video, superb skills, but no way it helps me.
@phillipchambers8487
@phillipchambers8487 5 лет назад
Great Video. More great Ideas to upgrade the HF Press. You're well on your way having a good Press for not much money.
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks again. Consider documenting your journey. Everyone wins if you do. This community is incredibly generous with ideas, help, and support.
@phillipchambers8487
@phillipchambers8487 5 лет назад
@@DudleyToolwright That is great to know. Man I just wish youtube, and all these Videos would have been around 25 - 30 years ago, and I would be a lot further down the Machining road. now. Lol Keep up the good work.
@DudleyToolwright
@DudleyToolwright 5 лет назад
I agree wholeheartedly. Other guys videos like Tom Lipton over at Oxtools really helped me out when I was starting.
@SgtCude59
@SgtCude59 6 лет назад
awesome upgrade gave me some ideal to fix mine
@DudleyToolwright
@DudleyToolwright 6 лет назад
Thanks.
@kenabi
@kenabi 5 лет назад
the newer versions of this have boxed steel on the push bar instead of c-channel, there's a plate under the jack itself, and the top where the ram sits is a ring instead of the two fold channel from front to back. there's some improvements that can be made with the new model, but not as many need to be done.
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks for the update. Much appreciated. Harbor Freight does seem to want to iterate and slowly improve their products. Thanks again.
@dimik3855
@dimik3855 5 лет назад
The joy of working metal to make it fit just right with what you've got at hand. Very inspiring! Now all I need is to get some more tools...
@DudleyToolwright
@DudleyToolwright 5 лет назад
Are there ever enough? I have a list of over 100 tools to make. Every time one comes off the list anther few go back on. I'm happily loosing this war...
@jimosborn5400
@jimosborn5400 6 лет назад
Great machine work! I don't have the tools or skill to do anything like this. I do have 1 little idea for your shop press. On the very top of the press I installed 2 broom spring clips to hold the handle for the jack so it wouldn't stick out, or get misplaced.
@DudleyToolwright
@DudleyToolwright 6 лет назад
I like the idea, Thanks.
@mikenixon9164
@mikenixon9164 6 лет назад
Good video. I make my knobs with a spindexer & a ball end mill works well
@DudleyToolwright
@DudleyToolwright 6 лет назад
I love the solution. Necessity is the mother of invention. I really love the lateral thinking going on out there.
@padraicmcguire108
@padraicmcguire108 5 лет назад
Ive rebuilt several 20 and 50T jacks. Getting them apart requires a huge pipe wrench and a hand maul Instead of parting the cylinder, id have used a band saw and then faced it. I think suggest having the screw head hard faced. At 20T you will be close to the yield stress for the soft soft screw head and so subject to brinelling. A good welder can put 50 thousandths of hard steel on this to protect it. Better quality jacks are not painted together as this one was,
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks for the suggestions. I did not have a band saw when I completed this project, but I will remember your ideas, if and when this comes up again. I like the maul idea. I have to secure the workbench where my vise is attached better, because I could make it move all over the place. I also thought about a 1" impact wrench. I have seen miracle performed with them, like taking a pully of an alternator shaft. Thanks as always for being so helpful.
@silverbullet7434
@silverbullet7434 3 года назад
Nice upgrades,no way that push shaft would be very stable at high pressure. Your remake just made it five times more stable plus stronger. We've wrecked a couple of those presses in a repair shop having them twist and parts flying in the shop. Now it wasnt I who did it but I saw the remnants.
@DudleyToolwright
@DudleyToolwright 3 года назад
Thanks for the tips and warning. I appreciate you taking the time to help out.
@MikesGarage96
@MikesGarage96 4 года назад
If you ever decide to manufacture any of them knobs, id be happy to buy one from you! I hate using that handle to open the valve on mine.
@DudleyToolwright
@DudleyToolwright 4 года назад
Thanks. I will add your name to the list.
@ianmoone2359
@ianmoone2359 Год назад
Got to say that I think this is a masterful effort indeed. Would like to copy this for sure. 👍 It’s a shame they don’t come this way from the manufacturer, because all of the improvements make a lot of sense to me from an operator comfort / satisfaction point of view. Poor design soon leads to dissatisfaction if using it becomes a bug-bear. I’m after a shop press, never owned one - mostly for broaching internal keyways - but also pressing bearings in and out etc. I think this would be a great addition to my shop. Thanks ever so much for showing all your improvements, all well thought out & executed. I’ll have to subscribe now. 👍👍👍🇦🇺
@DudleyToolwright
@DudleyToolwright Год назад
Thanks for all of the compliments. I really appreciate them . This community is great about sharing ideas and improvements. I just wanted to play my part, because I have benefitted so much from other's outstanding work.
@sanfordrhudy774
@sanfordrhudy774 8 месяцев назад
@DudleyToolwright Man, I wish that I had all of the machinery like you have. But, all of that machinery wouldn't be worth a darn without your skill. So,,,to go along with all the machinery, yup,,,I also would like to have all of your SKILLZZZ!!
@WireWeHere
@WireWeHere 5 лет назад
There's a potential consideration I would like to mention, bottle Jack's can be modded to work right side not up. The acme thread clearance adjustment shaft does then appear, as luck would have it on occasion, pointing the way of the udder. Good day and I'll watch for more of your, how it should have been done, videos.
@DudleyToolwright
@DudleyToolwright 5 лет назад
Others have mentioned this as well. I was not aware of this at the time, so thanks. I have tons to learn and I appreciate you helping me along.
@WireWeHere
@WireWeHere 5 лет назад
@@DudleyToolwright making a wheel for your main Jack's acme shaft is another possibility although you will be working against the two springs. I lost those in favour of counter weights encased in the stanchions. It's never ending. Have fun.
@donnatalielucasheimbigner7598
@donnatalielucasheimbigner7598 4 года назад
Like I stated in another video, I made D shaped handles from 1/16" x 1" flat for the cradle shafts to make them easier to work with and installed a cable winch & pulleys to move the cradle up & down much easier, particularly useful when adjusting with a work piece in the press. Otherwise, excellent ideas.
@DudleyToolwright
@DudleyToolwright 4 года назад
Great tip! Thanks for sharing your ideas. I could really use a pulley system to raise and lower my cross bars.
@donnatalielucasheimbigner7598
@donnatalielucasheimbigner7598 4 года назад
@@DudleyToolwrightThanks. That is the awesome thing about the net. People can share all sorts of information so everyone can benefit.
@charlesdevore7271
@charlesdevore7271 Год назад
Considering the design limits of the 20 ton press I am wondering if limiting the input pressure to the air over jack to 90 psi would de-rate it to around 17 tons?...oh yes I did drill those extra column holes and that came out well
@DudleyToolwright
@DudleyToolwright Год назад
I think that limiting the air pressure would work. Nice idea.
@bryankirk3567
@bryankirk3567 5 лет назад
On testing the Half-ball-bearing valves on old Rolls-Royce jet engine fuel valves, the test pressure was 2000 bar kerosene. More than enough to cut the end of a finger clean off, which it did to one of my colleagues, much to our delight.
@bryankirk3567
@bryankirk3567 5 лет назад
Mistake was made! It was 200 bars of kerosene pressure. Sorry
@DudleyToolwright
@DudleyToolwright 5 лет назад
That was a fascinating if not terrifying story. Thanks for the contribution. I had heard a story from an electrician that had worked building oil refineries and he was told that a pin hole in the ultra-high pressure hydrogen line had cased the decapitation of a worker who had walked through the nearly invisible jet. Respect high energy systems.
@PeterHatch-mx7zc
@PeterHatch-mx7zc 4 года назад
Thank you I injoy youf videos
@DudleyToolwright
@DudleyToolwright 4 года назад
Thank you for watching.
@PeterHatch-mx7zc
@PeterHatch-mx7zc 4 года назад
@@DudleyToolwright watching one now
@imknot
@imknot Год назад
I always seem to find videos that I want to comment on years after they have been posted. A thought on why the screw isn't hardened is that hardened parts are "slippery" there is no give to the surface so other hard parts can't dig in and will have a tendency to slip off. That's not a good thing when jacking up heavy items that don't engage the grooves machined into the top of the screw.
@DudleyToolwright
@DudleyToolwright Год назад
That is an excellent observation. Thanks, you are never too late.
@vinmaga6417
@vinmaga6417 5 лет назад
Nice upgrade
@DudleyToolwright
@DudleyToolwright 5 лет назад
I has worked out quite well so far, thanks.
@MaturePatriot
@MaturePatriot 6 лет назад
Put a match to it, see if it burns. LOL - Press out the plug. Yes/No? - Spindexer and ball end mill would have worked for handle scallops. - Did you mill a flat on the shaft where you brass bushing contacts the shaft? - It's different from other adjustment modifications I've seen. Hope to see it in use.....soon. Great work, and video.
@DudleyToolwright
@DudleyToolwright 6 лет назад
Which plug are you talking about? The oil drain? Spindexer was my first thought, but I got lazy and didn't want to pull off my vise, so tried to make that work. I think your suggestion is much better than what I did though. I didn't show it, but the work piec moved before I got the big handle for my vise (I usually use a speed handle). I considered a flat, but didn't want to compromise the ram in any way. It holds very firmly though, as is. Thanks for the continued support. I really appreciate it.
@MaturePatriot
@MaturePatriot 6 лет назад
13:40 The cast iron plug in the cut off end of the ram. Now that I look at it again there would be nothing to support it while pressing, as it over laps the end of the tube.
@DudleyToolwright
@DudleyToolwright 6 лет назад
True. I was originally going to use it as a keeper between the 2x4 tube and the plate. Instead, I used friction.
@drickard67
@drickard67 5 лет назад
@@marianoaldogaston the kerosene I lit with a match yesterday must've been defective.
@whidbeyman
@whidbeyman 6 лет назад
Pressing shaft is called a ‘ram’. I like the mods. Technical name for male bosses concentric with a part is ‘spigot’,
@DudleyToolwright
@DudleyToolwright 6 лет назад
Very strange that. I couldn't remember the word, "ram" until I finished the video. The word spigot on the other hand, I was never familiar with. Thanks as always.
@rednek40
@rednek40 4 года назад
Nice mods, maybe you could add a gauge to the ram somehow. At my job we have a 50 ton and a 20 each with a gauge. I like the idea of knowing how much pressure (psi) is applied. FYI for cuts and scrapes super glue is your best friend. Clean said cut dry and apply small amount to cover area. Brake cleaner will find any cut. the glue will protect from dirt grease out. just peel glue off when finished working to clean up.
@DudleyToolwright
@DudleyToolwright 4 года назад
I have thought about that and I agree it would be really useful. All you need is pressure in the ram and the ram surface are and you can calculate the rest. Thanks for the tips. I do use superglue upon occasion. It really can work well. Electrical tape also works in a pinch.
@PeterHatch-mx7zc
@PeterHatch-mx7zc 4 года назад
Can I come and work in your shop !! Great video
@DudleyToolwright
@DudleyToolwright 4 года назад
Thanks.
@keithharmon2056
@keithharmon2056 5 лет назад
great job Brother, I have this same press. You have some great ideas here I may use some of them.
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks. I appreciate the comment.
@danielleonte8464
@danielleonte8464 5 лет назад
That's the best press I ever seen!!!!
@DudleyToolwright
@DudleyToolwright 5 лет назад
Very kind, thanks.
@jmwarden1
@jmwarden1 6 лет назад
Watch pressing on that press plate that comes with the press, you can break them pretty easy and they shatter, I know I did it to mine.
@DudleyToolwright
@DudleyToolwright 6 лет назад
Thanks. you are the second person to comment on that. I will definitely watch out.
@optimumperformance6998
@optimumperformance6998 6 лет назад
The newer presses come with flame cut plate, the old ones (orange ones) were a casting and they break LOL.
@sawz5
@sawz5 5 лет назад
machining brass is like magic alright it gets to places you think are impossible!
@DudleyToolwright
@DudleyToolwright 5 лет назад
Every tool presents a whole new world of possibilities to me. I'm an addict.
@rogerthetinker5116
@rogerthetinker5116 6 лет назад
I was surprised that you did not make the side tangs ( the pieces that you welded on ) a little taller to keep the twisting front to back down.
@DudleyToolwright
@DudleyToolwright 6 лет назад
I haven't used the press that much yet, but I haven't seen any twisting issues. I will keep my eyes open now. Thanks.
@optimumperformance6998
@optimumperformance6998 6 лет назад
One suggestion would be to take the frame over to the mill and bore a pocket into your 3/4" plate as a 3rd register to locate your pusher screw
@DudleyToolwright
@DudleyToolwright 6 лет назад
Interesting idea. Thanks a lot. I appreciate you taking the time to give me great ideas.
@11YeeP11
@11YeeP11 Год назад
I only wish I had a mill and a lathe so I could do the same thing. I think I can come somewhat close and not as sexy looking. Question for you: Can you show some examples of the tools that you would make to attach to the new ram head? (I think that is what you call the rod that presses in side the press). I may have to see if I can get mine turned down to a perfect circle so I can do the same. Nice job, subscribed.
@DudleyToolwright
@DudleyToolwright Год назад
Thanks. I did these videos quite a while ago, but didn't I show making an adapter in at least one of them? All I did was bore out a piece of 4140 to the proper diameter and added some Allen screws just for friction to hold it in place. Thank you very much for the sub.
@EcoMouseChannel
@EcoMouseChannel 6 лет назад
I too have some press upgrades currently going on. Never gave much thought to that pusher pin ram thing. I may have to address that, since I'm upping mine to a 30 ton air/over hydraulic, with additional gussets, boxed in supports etc.
@DudleyToolwright
@DudleyToolwright 6 лет назад
If you are making a video, I would love to see your take on improving this press. I did consider going to a 30 tone jack, but was not comfortable with Harbor Freight gear having enough safety margin to pull it off. You approach sounds wise. I look forward to seeing it. I have sub'd. Thanks.
@EcoMouseChannel
@EcoMouseChannel 6 лет назад
Well, I guess I'd better make sure it turns into a video! See, the way I figure it, is that I'm not going to max out to 30 tons, but with a modified press brake, it'll make bending 1/4" plate for tabs and brackets that much easier and quicker. That's kind of the limit I work with in the shop anyway, based on max welder penetration (without having to do multi-pass welding) But yeah, on the docket is DOM tube spacers welded in the side legs where the pins go. Then fully box that C-Channel. Obviously, use grade 8 bolts everywhere... which I think I've already upgraded. Then on the platform, fit in little vertical gussets on the C-Channel, both sides, then box that in. Then on the upper part of the press, more vertical ribbing, and weld the open portion closed. I've not yet decided how I'm going to do that. Initially, it seems like you'd just slap a piece of 1/4" plate across the top. But the more I think about it, I'm leaning towards a piece of C-Channel in the down position. I've got my foot actuated pneumatic switch for the ram. Then I'll mount the whole thing to a mobile base. The last part is to find chainmail to make a front and rear curtain.
@DudleyToolwright
@DudleyToolwright 6 лет назад
It sounds like you are really going to end up with a nice press. You have me intrigued. I look forward to seeing a video(s) if you make them.
@EcoMouseChannel
@EcoMouseChannel 6 лет назад
Yes, I'll have content recorded for it as I go. I'll also most likely post on my instagram for sure though @EcoMouseDesign (I upgraded my HF gantry crane in much the same way. All grade 8 hardware, and an entirely new longer, stronger I-beam. So, I'll definitely be documenting the press build)
@DudleyToolwright
@DudleyToolwright 6 лет назад
I will check out your Instagram page and wait for the press build.
@darrenanton2898
@darrenanton2898 6 лет назад
Thats a good Project ! Love it!
@DudleyToolwright
@DudleyToolwright 6 лет назад
Thanks.
@kimcurtis9366
@kimcurtis9366 4 года назад
Question. Would it not have been better to mill a piece of hardened steel round bar and insert it inside the hollow tube, either welded in or press fir to give the whole assembly the strength you are looking for? That would eliminate ANY chance of it failing or deforming in any way. Just a LATE suggestion as I am just now seeing this video! I subscribed after viewing the first of these 2 videos. And will continue to watch your uploads! Thanks for the information! It was good to watch the process as you went through it. Also, I now, know how HF bottle jacks are made! Thanks, again for the videos. They've been very informative!!!!!
@DudleyToolwright
@DudleyToolwright 4 года назад
The 7075 aluminum is as strong as common coldrolled steel and so far I have not had any issues with deformation. However, I like the idea though.
@jeremiahperez1
@jeremiahperez1 5 лет назад
Great work! Great informative video
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks.
@johncooper4637
@johncooper4637 5 лет назад
I have no idea of what you are using for a camera so I don't know if you have a manual focus mode. Other than that the photography is excellent. I think I would have put a recess in the plate under the jack for the shaft and clamped it at that point rather than in the middle of the 2 x 4 tube which would give the shaft even more support. I would have run the shaft up into the plate and then bolted the plate to the 2 x 4 so that every thing was in alignment. Knowing that the shaft is not truly round I think I would have tried to true it up on the lathe. I'm going to see which of your modifications I can use on my HF 12 ton as I do not have room for the 20 ton unless I build a smaller work bench. I'm also building a stand for a 6 inch Buffalo vise (came with the Bridgeport I bought at auction and replaced with a DX6 as soon as I had the money) that will bolt to the floor for my rod bender made from Tom Lipton's plans. It will be handy for removing jack parts, too. I've disassembled several rusty jacks to use the pistons for mill clamp supports. They were older than yours and did not have paint holding them together so I was able to get them apart with very large pipe wrenches.
@DudleyToolwright
@DudleyToolwright 5 лет назад
My camera does not have manual focus mode. Very interesting suggestions thanks. The adjustable ram makes side contact at the top and the bottom of the 2x4, but Your idea might just be better. I considered your approach, but thought that my current method would be ok. Time will tell. As a side note, I did later true up the roundness of the shaft. You might consider making some vids. I would be interested in seen the projects you have outlined. Cheers.
@robertgoldsteen604
@robertgoldsteen604 Год назад
Great ideas to upgrade my Chinesium press, I have ordered an air/hydraulic jack. A pressure gauge would be good, but how to do it?
@DudleyToolwright
@DudleyToolwright Год назад
That is a good question. You would need the pressure in the piston, which isn't too easy to access. Interesting problem.
@shaunkijak2571
@shaunkijak2571 5 лет назад
Bad ass. You've earned a subscriber. Can you please make me a bleeder screw knob! I love that feature!
@DudleyToolwright
@DudleyToolwright 5 лет назад
You aren't the first. If I ever get a CNC machine I will crank some out. Thanks for the kind words.
@97JoMiller
@97JoMiller 5 лет назад
you should make yourself a holder for your jack rod, I find it annoying how often mine falls.
@DudleyToolwright
@DudleyToolwright 5 лет назад
Excellent point and I think I will.
@charlesdevore7271
@charlesdevore7271 Год назад
On my application drilling additional 21mm holes on the 2 column uprights inline and halfway between the existing 4.5" center holes would allow adjustment for my 2 sets of dies,,has anyone drilled holes in that manner, any ideas of structural results,,?
@DudleyToolwright
@DudleyToolwright Год назад
I don't know, but I understand the idea. I think the designed hole spacing was chosen based on ram travel length so that you could get full range coverage. I would carefully consider doing anything that potentially makes the column weaker. After doing my pressure testing of this hydraulic press, Harbor Freight seems to have had, at least some parts, made without much of any safety margin. When testing the press at full capacity (20Tons) the top bar of the press deformed permanently. Failures in high PSI environments can be catastrophic, so please be careful.
@gymedude
@gymedude 6 лет назад
You know that nicely honed outer tube that you saved and liked so much during initial tear down. Why don't you cut it down and insert inside the rectangular tube to add reinforcement at distortion points that will arise as force is transmitted through your (piston shaft) new press pin. This is not criticism, I really like your idea and applaud your creativity by not just scrapping a worn tool but using it to make something better. I think it would add a lot of strength to the rectangular tube where the piston rides against. Still, it is thick, it would be nice if you could update function/wear after a few years of use.
@DudleyToolwright
@DudleyToolwright 6 лет назад
Thanks. I appreciate the suggestions. The ideas a great. I will let you know how well the press has faired over time. I am using it more, recently. I have some broaching jobs ahead, so time will tell. Thanks for sharing your ideas.
@ypop417
@ypop417 6 лет назад
I would thread the old ram for ironworker nut and use it for punching making a die holder plate for the bottom.
@DudleyToolwright
@DudleyToolwright 6 лет назад
Nice suggestion. I will have to do some research to understand the details of your suggestion, but it sounds great. I have very little experience with presses and even less with iron workers so I get the drift, but would like to understand the specifics better. Thanks for taking the time to share your thoughts.
@ypop417
@ypop417 6 лет назад
You are welcome. You would not be able to punch too thick of material. thinking 1/2" in 1/4" little rusty on tonnage for thickness
@DudleyToolwright
@DudleyToolwright 6 лет назад
Thanks. I had no idea such a small press could punch holes that big in material that think. Amazing. I realize that you are spit balling, but wow.
@ypop417
@ypop417 6 лет назад
americanmachinetools.com/tonnage_punch_hole.htm I was wrong it's 1/2" in 1/2" 20 tons that assuming everything is sharp.
@kevinmcguire3715
@kevinmcguire3715 Год назад
You mention that Harbor freight did not do a careful job machining the jack ram. It looks like you use a 4 jaw independent chuck . Why did you not indicate the ram while installing it in the 4 jaw chuck? Or, is the ram slightly bent from pressing stuff?
@DudleyToolwright
@DudleyToolwright Год назад
You make a good point. I was just facing off the face, but it could have ended up crooked in the jaws with the final face not perpendicular to the shaft axis. I should have.
@Garth2011
@Garth2011 6 лет назад
Thanks for the ideas. Also, love the machine room dictionary word "craptastic".
@DudleyToolwright
@DudleyToolwright 6 лет назад
I can't remember where I heard the word, but I immediately loved and adopted it. Cheers.
@Garth2011
@Garth2011 6 лет назад
Yes, I hear it mostly from machinist and mold makers.BTW, I noticed Harbor Freight has a Central Machinery 20 Ton Industrial that has the air motor, in the mid $200's price. Painted Orange.
@DudleyToolwright
@DudleyToolwright 6 лет назад
Interesting, I wasn't aware, nor have I seen it. Thanks.
@Garth2011
@Garth2011 6 лет назад
I think it's marketed to crush oil filters but it's still a 20 ton frame so it's not as tall some have reported, around 3 feet tall. If so, no big deal to raise it up to standing height.
@billybobsowbreath1774
@billybobsowbreath1774 4 года назад
I like the adjustable ram. Yes, the original setup on these presses aren't that great. I'm always trying to find the right-sized widget to take up space to press something. I keep a bucket of cut-offs for just this reason. I thought of taking mine apart and drilling/tapping that ram. Something.. ANYTHING that would make it adjustable. Your idea is better to replace the whole thing. I might steal this from you if I run across an old bottle jack. I also like to recycle old tools into something new. Just something about having a big press makes you feel all warm and fuzzy doesn't it? LOL!
@DudleyToolwright
@DudleyToolwright 4 года назад
Yes it does. I don't need it all that often, but when you do it's really handy. I use the arbor press for most small things.
@markalbrecht2444
@markalbrecht2444 5 лет назад
Love your videos , keep them coming!!
@DudleyToolwright
@DudleyToolwright 5 лет назад
I will try. I found machining a bit late in life, but now I am hooked. Thanks for the comments.
@patbarrett9263
@patbarrett9263 5 лет назад
the internals of yours looks a lot better than my jack mine was full of rust
@DudleyToolwright
@DudleyToolwright 5 лет назад
I wish I could say that I am surprised.
@johnfry9010
@johnfry9010 6 лет назад
Pimp my Press , Nice work !
@DudleyToolwright
@DudleyToolwright 6 лет назад
Thanks.
@Railsplitter21
@Railsplitter21 2 года назад
I am curious how you made the hand turn knob on the bottle jack?
@DudleyToolwright
@DudleyToolwright 2 года назад
I made it on my lathe, which puts this part out of reach for many, but there are some other really creative solutions out there.
@joesbarbecue1
@joesbarbecue1 7 месяцев назад
I was considering this mod, except I don't have a lathe. So then I thought about buying one from harbor fright, but then I began to wonder how many videos and mods I'd have to go through to make that operational. By the time you get done with all the mods on one of these presses, I'm about to believe it'd just be best to buy a quality one and be done. On the other hand, wouldn't it have just been easier to cut off the shaft on the press and attach the second jack upside down?
@DudleyToolwright
@DudleyToolwright 7 месяцев назад
I get your take, but the equivalent high quality 20 ton press goes for $3-5k. It would be a whole lot better, but quite expensive. Flipping a jack upside down is a really good idea, but in order for it to work you have to take it apart to modify it so that the hydraulic fluid pick up comes from the other side of the reservoir. Definitely doable.
@joesbarbecue1
@joesbarbecue1 7 месяцев назад
@@DudleyToolwright Actually my thought was just being able to screw the shaft out in order to take up the slack in certain situations and save a whole bunch of pumping.
@larryschweitzer4904
@larryschweitzer4904 5 лет назад
Nice mod. I have a 20 ton Chinese bottle jack press I bought a long time ago. The presser foot attachment is not perpendicular to the travel. I faced the foot but that of course didn't fix the problem. It is just held on by a set screw so no rotary reference. Will change that. I had been considering making a threaded foot extension on the lathe but your solution seems better. I want to make some adapters to fit the presser foot. This older press is quite a lot heavier made than the newer ones but still sloppy in it's travels. It came with two very soft, very irregular bars of steel for the pressing surface. I machined them flat and square edged but they get dinged up very easily.
@DudleyToolwright
@DudleyToolwright 5 лет назад
Interesting, thanks. The softer press plates may deform and gouge, but that might be a bit better than the ones they made out of cast iron that fail catastrophically. I have had a bunch of people warn me about them, although the way mine machined, I don't think they are cast iron. If you video your improvements, I would enjoy watching.
@larryschweitzer4904
@larryschweitzer4904 5 лет назад
I don't have a video camera. Can do photos. I bought a used Jet mill about 4 years ago. 2 years ago I bought a new PM1440HD Chinese lathe. It's OK. I've been learning machining VIA the RU-vid university. The two best sites I've found are Joe Pieczynski's and Thatlazymachinist. Both excellent educational value. Would like to trade e-mails about our mis-adventures in machining. I also do some Aluminum casting. Best videos for that are from olfoundryman. Interesting videos from myfordboy include some casting and machining.
@DudleyToolwright
@DudleyToolwright 5 лет назад
Good recommendations. Some other really excellent teachers are Oxtools with Tom Lipton, ABOM 79, Keith Fenner, MrPete222, and ROBRENZ (master of precision). Tom was my inspiration to start learning this trade. He explains his thought processes when he machines, a born teacher.
@larryschweitzer4904
@larryschweitzer4904 5 лет назад
@@DudleyToolwright -- I don't have video capability. Over the last week I've been trying to tune up my lathe and mill. I started on the lathe by using a test bar to get the collet chuck as close to centered as possible. It is Chinese made with the "set true" design. It appears to be very nicely made. My collet set claims to be with in .0005". So trying to get any better runout on the chuck is a waste of effort. I managed to get .0002" with the collet and test bar I was using but that figure is only good for that particular set up. I use the collet chuck more than I ever thought I would. On work up to 1.125" it is quicker for me to be able to swap ends of the work than using a 4 jaw. I'm no Abom79! I did get my mill trammed in the left rt. direction pretty much dead on. Now I've got to try the nod direction.
@nathanwarner4333
@nathanwarner4333 5 лет назад
Great video, I will do some of the same things or sort of !!!! Thanks
@DudleyToolwright
@DudleyToolwright 5 лет назад
Thanks. If you end up doing things differently, please share. We can all benefit.
@josepeixoto3384
@josepeixoto3384 4 года назад
I watched both, thanks for showing us, fully agree with the improvements,i would do the same,*but* ,just curious, with all that expensive machine shop equip' there, why didn't you just get a proper 20 ton press in the first place,with a real ,a fat one, 20 ton jack ? You sped up that jack, maybe you do *a lot* of pressings? if so,a good 20 ton press would make sense; if not,speeding up the jack(expensive!) is the only thing i would not have spent extra money on; the bottom threaded adjustment is gonna make me wish my press had one lol
@DudleyToolwright
@DudleyToolwright 4 года назад
I loved the challenge and I really do have limited funds and have to pick and choose carefully, the items I buy. Also, I am always looking for content for my channel, that might help someone else.
@inerlogic
@inerlogic 5 лет назад
Would it have been cheaper/easier to machine your own presser shaft, cut the acme thread, etc, rather than sacrifice a working jack? For support, would it make sense to cut a small cup in the base plate? So the shaft is supported on the end by the cup and the two wall thicknesses....
@DudleyToolwright
@DudleyToolwright 5 лет назад
Interesting take. I will have to think more about your suggestions. Thanks. I had zero used for another spare jack, so I was not worried about killing the one I salvaged. However, it would have been an interesting project making a presser shaft as you suggest. Cool.
@portocal1976
@portocal1976 Год назад
Great job is there way to order all this great improvements for me? Thanks
@DudleyToolwright
@DudleyToolwright Год назад
Thanks. I am afraid that as a manual machinist these parts would have to be too expensive to be worth it for the consumer. If I ever decide to make a batch, I will let you know. The other problem is that Harbor Freight constantly changes their products, often having multiple SKUs for a single item, like this press. If I made parts for one, they might very well not fit another.
@portocal1976
@portocal1976 Год назад
@@DudleyToolwright Thanks anyway … if some day decide to make it … I’ll be happy to have it Have a nice Sunday
@BDuck-lp2pg
@BDuck-lp2pg 2 года назад
I'm interested to know what the ID was on the bottle jack ram and if it would have been possible to just slide it over the existing piece that was provided by the manufacturer? Might be an easier way for those of us that don't have machines to make all of the machining changes that you made.
@DudleyToolwright
@DudleyToolwright 2 года назад
I appreciate the question. I always try to reply to every comment. It has been several years since I made these mods and I did not keep the original fixed ram and crosspiece. As I recall they were very similar in diameter, but I am not entirely sure. I really like your approach to the solution. You definitely could reduce the diameter of the fixed shaft to fit inside the one I removed from the jack that came with the press. It would require a large lathe of removal and then it would need to be rewelded to the crosspiece. I suppose with a bunch of effort you could manually reduce the diameter. Your approach is a novel one. A bigger problem for me to comment is that Harbor Freight changes their product manufacturers all the time and often has multiple SKUs for current products, so I have no idea if my observations currently apply. On a positive note they seem to be incrementally improving their tools.
@eddietowers5595
@eddietowers5595 6 лет назад
Great video. Cool project. Oh yeah, ram [piston] the hydraulic cylinder, to push, is a ram.
@DudleyToolwright
@DudleyToolwright 6 лет назад
Yea, it was weird. The whole time I was making the video, I couldn't remember the name for the "ram", until I was editing it. Go figure. My brain works strangely with word recall. Thanks for the help. I really appreciate it.
@eddietowers5595
@eddietowers5595 6 лет назад
No worries, the brain is a fickle machine, the whole point was the project, but i’ll Lend a hand when it’s needed. Thanks for sharing cools vids.
@DudleyToolwright
@DudleyToolwright 6 лет назад
Much appreciated.
@metalworksmachineshop
@metalworksmachineshop 5 лет назад
Nice work. Youll also at some point want to make the two plates , black ones .. flat.
@DudleyToolwright
@DudleyToolwright 5 лет назад
You were not the first to comment on the press plates. Apparently there were a lot of issues with the plates breaking catastrophically in the past. Thanks for the comment.
@joeport6823
@joeport6823 6 лет назад
You could have clamped one of your lathe chucks on the milling table to hold your part.
@DudleyToolwright
@DudleyToolwright 6 лет назад
You are the second person to recommend this excellent and now obvious suggestion. Thanks.
@ghilreese3413
@ghilreese3413 6 лет назад
Nice press videos. Swag off road makes press plates to replace the HF ones. Thanks for the videos.
@DudleyToolwright
@DudleyToolwright 6 лет назад
Interesting. I was not aware they made press parts. I will check it out. Thanks.
@DudleyToolwright
@DudleyToolwright 6 лет назад
Boy they have expanded their offerings. Very cool.
@ghilreese3413
@ghilreese3413 6 лет назад
The Swag DIY press brake would be handy.
@DudleyToolwright
@DudleyToolwright 6 лет назад
It would indeed. They are really coming up with a bunch of great products.
@littlebriar
@littlebriar 5 лет назад
@@DudleyToolwright Old thread, but, I recently bought Swag's 20 ton press brake kit and their gooseneck dies. The kit was easy to fabricate and works great on my unmodified 20 ton HF press. I have used them several times. I'm thinking about getting their arbor press brakes but they are not cheap. Loved both videos on the project and will do something similar on mine when the weather warms up in my unheated, Michigan shop.
@JasonAguirre
@JasonAguirre 4 года назад
When I assembled one of these today, I noticed the vertical frame doesn't actually touch the base of the feet. It's just resting on the bolts. There are also four struts at the bottom that are suppose to keep it from wobbling, but the two pieces they bolt into aren't on the same plane so the strut has to flex to be tightened. It all seems fixable but haven't noticed anyone mentioning it so wondering if I just got a crappy unit.
@DudleyToolwright
@DudleyToolwright 4 года назад
Harbor Freight seems to source their tools from multiple vendors, so they are all different. When I bought mine, there were three different part numbers that different stores carried. In your case there is not much force on the base so it seems like you'll be okay. Nice information for the community.
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