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Grinding the main shaft on the CNC Machine --Part 3-- Old drillpress restoration 

Alex CNC en
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In todays video I will fix the stuck quill again. Last time I didn't noticed another problem with the quill. Therefore I have to disassemble the quill again and grind down the shaft on the CNC Machine so it can slide freely in the main pulley.
I hope you liked the video. If that's the case don't forget to like and subscribe :)

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27 авг 2024

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Комментарии : 18   
@AlexCNCen
@AlexCNCen 5 лет назад
German Version over here! ru-vid.com/video/%D0%B2%D0%B8%D0%B4%D0%B5%D0%BE-MhaDv9aBqR0.html
@arnljotseem8794
@arnljotseem8794 5 лет назад
clever set up for the grinding. That is the fun part about shop work. Finding solutions with the tools and material you have at hand. Nice video Alex, I really like your channel
@bojansar1
@bojansar1 5 лет назад
I really like your videos,glad to see that you make English version now.
@morksbeanbag
@morksbeanbag 5 лет назад
Excellent work and very informative Alex, looking forward to more videos.
@Toonces311
@Toonces311 4 года назад
I want to add my appreciation. Your videos are excellent. Thank you for the time it takes to make them as well as the precision craftsmanship your are willing to share will us.
@TrPrecisionMachining
@TrPrecisionMachining 5 лет назад
Great video again man...Thanks for sharing
@KravchenkoAudioPerth
@KravchenkoAudioPerth 5 лет назад
Great video Alex. I enjoy watching your adventure in rebuilding this drill press. THanks for taking the time to make this video. I know it takes a lot longer too make a video and do the work. Mark
@RaptorMachineToolCo
@RaptorMachineToolCo 5 лет назад
Great job. Thank you!
@cpirius
@cpirius 5 лет назад
That's a hell of a setup :) I like it
@What-is-thehandle
@What-is-thehandle 5 лет назад
Great video Alex! Do you think a tail stock would have helped? Or do you think it would have increased the run out?
@AlexCNCen
@AlexCNCen 5 лет назад
Alignment would have been very difficult. There are no surfaces to check the correct alignment. The setup was rigid enough to get good results. And that's not a milling spindle or something like that with preloaded bearings. This one just has normal ball bearings in the back. Therefore the 2/100mm runout after grinding was very good :) Best Alex
@AlexCNCen
@AlexCNCen 5 лет назад
I used a very similar method to grind the BT30 taper of my milling spindle. Only difference was, that the grinding bit was mounted horizontally. There I got unter 2μm runout in the spindle taper. So it's definitely possible to get very accurate results!
@AdamEarl2
@AdamEarl2 5 лет назад
Clever way to grind a shaft! Was there a lot of wear on the wheel after doing this?
@AlexCNCen
@AlexCNCen 5 лет назад
There was a little bit of wear. I think mostly from the keyway "cutting" away the grinding bit. It would have been better to mount a bigger grinding wheel horizontally. Then it would be no problem to grind away a lot of material and the finish would have been better. Best Alex
@DUIofPhysics
@DUIofPhysics 5 лет назад
Yeah, when it comes to grinding, it's best to have your wheel perpendicular to the feed axis so that the edge of a wheel gets used up first, that way you know when your wheel is 'spent' as your whole wheel is dirty, or 95% of it is. The moment your entire wheel circumference is dirty, you're no longer grinding to the correct distance.
@airtightbox
@airtightbox 5 лет назад
You should check out Keith Fenner's channel he has put up some videos on the topic of heat straightening bent shafting, it's pretty amazing what can be done to true up a shaft.
@AlexCNCen
@AlexCNCen 5 лет назад
Thanks for the tip. I have already watched some videos from Keith but haven't seen the ones about the shaft straightening. Best Alex
@bobdickweed
@bobdickweed 5 лет назад
Great video again man...Thanks for sharing
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