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Making a New Cylinder for the 3D Printed Gas Engine (so it runs, like, properly) 

Camden Bowen
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okay I guess it's not really a 3d printed gas engine anymore but when does a hill become a mountain anyways
Big thanks to PCBway for sponsoring today's video: www.pcbway.com
Instagram: / bowen3dprinting
Patreon: patreon.com/user?u=84920684

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30 апр 2024

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Комментарии : 880   
@MeriaDuck
@MeriaDuck 14 дней назад
Love how this project evolves from 80% 3d printed plastic parts to like 20% 😂
@user-yz8do8vu1s
@user-yz8do8vu1s 13 дней назад
almost as if plastic is not a suitable material for combustion engines.
@Lenevor
@Lenevor 13 дней назад
@@user-yz8do8vu1sit isn’t?
@DevinSloan
@DevinSloan 13 дней назад
@@user-yz8do8vu1s how could we have known this!?
@lucasguythebest
@lucasguythebest 13 дней назад
fire + plastic = melt, who would have wonderd?
@mkosmo
@mkosmo 13 дней назад
the 3d printed parts were still critical to its development, so I think it still counts.
@benhoward2619
@benhoward2619 13 дней назад
I think you’ve officially gone from “building a 3D printed engine” to “building an engine”!
@thecrazyinsanity
@thecrazyinsanity 13 дней назад
still interesting but its 3d printed in the same way a gun is, it doesn't need any precisely made parts just some lightly machined metal
@edvinjohansson9625
@edvinjohansson9625 14 дней назад
You need to rejet the carb. if you take the bowl off you will find two jets. One right under the throttle, called the main jet, and one in front called an idle jet. Turning that screw does basically nothing, and is only really meant to fine tune it at idle. The main jet limits fuel at high throttle, the idle jet limits fuel throughout the range. You need to go up a size or two in idle jet, and a few sizes in main jet. The needle can also be moved up or down to give it more or less fuel, and sometimes you need to change the needle out for one with a different shape in order to fine tune it so it runs good at all throttle openings, loads and rpms. Properly tuning a carb is an art, but getting it good enough to run ok is easy
@theLyzhendricks
@theLyzhendricks 13 дней назад
This
@johndaniels1344
@johndaniels1344 13 дней назад
Agreed
@Handyman1199
@Handyman1199 13 дней назад
Very true. Seems like it’s running too lean since with the torch it starts and runs better, doesn’t accept any throttle (this carb has no accelerator pump, it’ll lean out for a short bit when giving throttle) and sometimes backfire
@iancampbell6002
@iancampbell6002 13 дней назад
Agreed but did anyone think about the carb not getting the right fuel...it is a gravity feed carb and look at how his fuel bottle is...gas isn't going to get sucked up out of that bottle without a fuel pump
@Handyman1199
@Handyman1199 13 дней назад
@@iancampbell6002 that could also be a reason for the lean condition. Unless he’s siphoning the fuel beforehand so it pulls itself out the line and into the carb
@f3rny_66
@f3rny_66 13 дней назад
I love the switch from freedom units at buying to metric for precision machining
@CamdenBowen
@CamdenBowen 13 дней назад
I'm from Canada so trust me, I hate imperial as much as the next guy ahah
@bz938
@bz938 13 дней назад
Imperial works fine for precision machining. 44.09 mm or 1.736". Either way, you're dealing with decimals. I prefer imperial just because it's more intuitive to me.
@murmaider2
@murmaider2 13 дней назад
the lathe is probably metric
@IANHANDS
@IANHANDS 12 дней назад
Imperial measurement was around before the land of freedom was stolen
@dman8734
@dman8734 11 дней назад
@@murmaider2 IDK if I'd trust the dials on the lathe tbh :D
@breme818
@breme818 13 дней назад
Crazy how the engine went from running on hopes, dreams, and starter fluid to actually being able to idle on just gas. The project truly has come a long way from the blocky plastic days
@99prxp
@99prxp 13 дней назад
just fyi, you can make the case 200% the current strength in the axis it's shearing just by rotating the print on its side
@CamdenBowen
@CamdenBowen 13 дней назад
I have no idea how I forgot about that
@Roy-al-Paign
@Roy-al-Paign 13 дней назад
I was thinking the same thing but I've never 3d printed. I have a feeling we will see that next episode.
@99prxp
@99prxp 13 дней назад
@@Roy-al-Paign if you want a semi-scientific breakdown of it cnc kitchen has a great series on alot of this stuff
@deathreus
@deathreus 8 дней назад
@@CamdenBowen Layer adhesion is the one property I always forget about with mechanical prints, it's okay
@NJP-Supremacist
@NJP-Supremacist 14 дней назад
Once it's complete, I think it would be cool to recreate the same thing but all metal.
@themuffinfish2091
@themuffinfish2091 13 дней назад
I've been working on a metal version of a 4 stroke similar to camden's. Hard to balance with exams and such but once the head is done I'll make a video. You better watch out
@judeackland-patel6646
@judeackland-patel6646 13 дней назад
@@themuffinfish2091 I'm an aero student trying to do the exact same thing. Having access to a machine shop is awesome but it's so addictive and I don't want my grades to nose dive any more lol.
@user-ft1ee7nn3n
@user-ft1ee7nn3n 13 дней назад
it basically already is
@lonesimba
@lonesimba 12 дней назад
guess by the time its complete it will be all metal
@StealthTheUnknown
@StealthTheUnknown 14 дней назад
Insta-liked faster than I ever have. Used to have a friend named Camden, he’s no longer with us. I miss him, he was a good man.
@stuntvist
@stuntvist 13 дней назад
9:44 after comparing to "3 Hours of Volkswagen 1.9TDI idling ASMR, relaxing sound", I can confirm that genuinely sounds almost exactly like a 1.9 TDI idling.
@CamdenBowen
@CamdenBowen 13 дней назад
My dad had one when I was younger that was passed around from person to person, by the time I was 16 I was supposed to have it as my first car, it had just shy of 600,000kms on it but the transmission died and I think it blew up its 3rd turbo. Cool cars though
@stuntvist
@stuntvist 13 дней назад
The fueling problem could be related to the acceleration pump (if those tiny ones even have those). It's likely just not getting enough fuel when you give it throttle and bogs down immediately when it gets fed more air. If you ever get that working I'd love to see you try and blow it up with nitrous afterwards lol.
@stuntvist
@stuntvist 13 дней назад
​@@CamdenBowenThe 1.9's are still around everywhere in Europe and 600k isn't even uncommon. Decently fuel efficient and easy to repair most of the time and the manuals can take a beating. Cheap to buy here and cool to mess around with. Seen some people get almost 500hp out of them but that's a lot of work and money to put in a Seat Cupra or lead brick Passat (the B5's have no business being that heavy) lol.
@danemclaren5678
@danemclaren5678 12 дней назад
I have one now, a 2000 Jetta with a manual transmission. it’s at about 475000km and going strong… in my opinion those were some of the best cars ever made. I’m pretty sure it’s on the original turbo and injectors
@nathaniel1207
@nathaniel1207 13 дней назад
Definitely look into adding a crank case ventilation valve or line, just so that you don't end up with the lower end being any more of a pressure bomb than it already is with the crank trying to force it apart
@camdenbaum3686
@camdenbaum3686 13 дней назад
“But I figure if there’s both fuel in the engine and in the fuel then I’ll be okay.” I haven’t ever laughed so hard at an engineering video I love it
@austinspor2558
@austinspor2558 14 дней назад
I studied machining in college, and it looks like you need some oil to lube up the cutter. The feed rate, which is turning speed and turning speed combined. Your turning speed depends on grade of medal.
@ZoomZoom8th
@ZoomZoom8th 14 дней назад
My college machining instructor taught to (essentally) never use oil with carbide tooling because you could thermally shock the insert and it would break/chip. If it's not cutting well, you're looking at a feed/speed problem or a lack of rigidity. Cutting oil was exclusively used with high speed steel.
@austinspor2558
@austinspor2558 13 дней назад
@@ZoomZoom8th then I guess it would be better to use coolant in instead. Which can be bought fairly easily.
@CamdenBowen
@CamdenBowen 13 дней назад
In the beginning I was using wd40 as a cutting fluid, but later I found out that an old bottle of power steering fluid worked surprisingly well
@austinspor2558
@austinspor2558 13 дней назад
You can find such coolant doing a simple Google search of "metal cutting coolant." For the best and cheapest way is a water solvable coolant that is used by most manufacturers.
@Roy-al-Paign
@Roy-al-Paign 13 дней назад
​@CamdenBowen I was wondering if there would be an improvement on the chatter if you sent the boring bar into the cylinder before making contact with the Inner bore. Then feed out of the pipe.
@aserta
@aserta 14 дней назад
8:08 My boy, you should go back in time. Engines were pretty much simple affairs back in the day. Sandwiching the bore between two plates with 4 bolts would've been sufficient. No need to weld as long as the fitment is good. 13:11 when you don't have the spreader tool, you just take a pair of scissors you don't like and cut hooks (facing outwards) into the ends. Those hooks hook into the ends of the ring and spread it. With one hand you spread the scissors and with the other you keep the ring aligned and guide it unto the cylinder.
@seniormika
@seniormika 13 дней назад
its too emotional to see her running 🥲
@kevinleee3408
@kevinleee3408 14 дней назад
You should consider getting an end mill. Then you can bore out a cylinder into a solid chunk of metal. You can also cut keyways. You could also make a connecting rod out of a solid chunk of metal using the mill
@chasegraham246
@chasegraham246 7 дней назад
This is the RU-vid I love most. No fancy 6-axis CNC machine, no fancy machinist certifications, just a dude with a $300 lathe, a cool idea, and a LOT of patience.
@Sir_Uncle_Ned
@Sir_Uncle_Ned 11 дней назад
That is OFFICIALLY an idle! Most people never get even remotely this far in their engine from scratch projects! Incredibly well done!
@CamdenBowen
@CamdenBowen 11 дней назад
Thanks for sticking around this far :)
@Sir_Uncle_Ned
@Sir_Uncle_Ned 11 дней назад
@@CamdenBowen Of course! It's been an amazing ride so far and I can't wait to see where it take us next!
@Maxwe1I
@Maxwe1I 14 дней назад
Genuinely underrated channel
@linuxguy1199
@linuxguy1199 13 дней назад
This series should be called "3D Printed engine becomes more and more metal"
@Nathan-gn1ni
@Nathan-gn1ni 11 дней назад
I’m a motorbike mechanic and specialise in classic and vintage 2 strokes and this is the first time I’ve seen someone put a 2 stroke piston in a 4 stroke set up ☺️ good on you tho for never giving up on the build 👍
@jwpx11
@jwpx11 8 дней назад
I love the bringus studios style editing, gets me every time
@kiraditt523
@kiraditt523 13 дней назад
That is so awesome, I've been wishing for years for someone on youtube to build their own engine, great job getting it to run.
@tombuster
@tombuster 13 дней назад
Finally seeing the engine run on gasoline is so impressive! Can't wait to see you incorporate more machining into projects! It was really interesting to see how much actually goes into making a lathe usable in the last video and how its quirks still show up... The world isn't ready for what you could create with a proper non-shaky lathe setup! I love how much I learn about engines just watching you build better versions each time! I had no idea about cross-hatching but it makes so much sense when you put it in context!
@benmcreynolds8581
@benmcreynolds8581 13 дней назад
Putting those bolts all the way through and down into the base was the ultimate final addition to your creation. It essentially clamped itself together. Rather Than explode itself apart from little plastic screw points. You knocked this out of the park. That lathe really came in handy
@magnusclapront947
@magnusclapront947 8 дней назад
I’ve been following this series and this is actually so inspiring, good work!
@RaisinBarXZ550
@RaisinBarXZ550 13 дней назад
I love this project, I've always thought about building an engine myself from scratch, and this series has taught me a lot for what I can do to make my life a bit easier
@Adam-zf3bv
@Adam-zf3bv 14 дней назад
I love seeing this series, I hope to see more iteration on this, I'd love to see you try to replace the remaining plastic parts with metal parts within the tools you have.
@shlushe1050
@shlushe1050 12 дней назад
Now it's time to get it to rev up higher! Excellent work!!!
@brennanbair5699
@brennanbair5699 8 дней назад
I wish I could do a project with you.This is cool stuff.Please keep going because you seem to be ridged despite many adversities.Thanks for the educational material
@najron7152
@najron7152 11 дней назад
Bro so cool! been watching this series from the story and I love how this eloves! I would really like to see atleast another video with this engine when you will upgrade it to its max so cool keep going! :D
@callummalseed7908
@callummalseed7908 13 дней назад
Thank you for keeping this series going. I've been so looking forward to it
@takumikid
@takumikid 13 дней назад
i would love to see this engine run without problems keep up the work this is amazing
@woody.503
@woody.503 14 дней назад
To fix that bogging, take out the slide from the top or the carb, and there’s a needle that you need to move up. That needle blocks the main jet so at any other throttle position than wide open, it’ll have about the same AFR.
@inthefreytoo
@inthefreytoo 13 дней назад
Awesome video! Thoroughly entertaining, enjoyable and informative. What more can you ask? Yes, you have figured out your personal, RU-vid "formula". I watched the whole thing! Good work! WANT MORE!
@stupidbush8656
@stupidbush8656 13 дней назад
Hell yeah I’m so glad you’re going with stronger materials and it’s actually working and running on gas love these videos also your voice is nice
@montaguemonro565
@montaguemonro565 13 дней назад
Hell yeah dude, nice work. love your engine vids!
@jooch_exe
@jooch_exe 11 дней назад
Damn exiting stuff. I'm totally in for DIY forged parts.
@balsamicboot5358
@balsamicboot5358 13 дней назад
Congratulations on completing this project. I’ve been watching since the beginning. Your videos helped me get through really tough nights alone when I was going through chemo the past couple years. Thank you
@CamdenBowen
@CamdenBowen 11 дней назад
It means a lot man that you would share that, I hope that things are going well with you man!
@xynomia
@xynomia 11 дней назад
I appreciate the amount of work it took to make this. Keep doing what you’re doing!
@Minty1337
@Minty1337 13 дней назад
i cant wait to see this engine actually doing work, running something, but i don't know what at this scale, maybe a motorized bike?
@Handyman1199
@Handyman1199 13 дней назад
I guess it would run into its limits powering an alternator to run a few incondecand light bulbs. In fact since Wattage and Horsepower are both measurements of mechanical performance he could hook as many headlight bulbs onto it as he can find and do the math (60W per Bulb, 1000W=1,36HP)
@Timsturbs
@Timsturbs 13 дней назад
run generator to power a 3d printer that will print a part for that engine. 3d printing engine.
@Minty1337
@Minty1337 13 дней назад
@@Handyman1199 i think a motorized bike would be easier than a generator since you can use momentum and start the engine after the bike is already moving, so it only needs like half a horsepower to maintain speed.
@pauljs75
@pauljs75 11 дней назад
@@Minty1337 I think the idea is to use the generator in lieu of a torque brake to see just how much power it actually makes. How much load before it stalls? Not necessarily as something to be the final application.
@Minty1337
@Minty1337 11 дней назад
@@pauljs75 im worried this thing will break very quickly, even in the final version, so i'd personally test something like this with the final application, since it'd probably explode while being tested as a generator like that. it would be more fun to have it explode after it did something like power a motorized bike, rather than a small generator.
@djbe3772
@djbe3772 13 дней назад
I appreciate all the hours of work put into just this video, let alone the whole series.
@boogiehasfun
@boogiehasfun 13 дней назад
amazing video, you are easily on my top 10 favorite channels. i wonder what comes next.
@gregbingaman2092
@gregbingaman2092 8 дней назад
Yes!!!!! Been following this project from the beginning and I gotta say I’m impressed asf!
@inconsisstence
@inconsisstence 13 дней назад
I never EVER thought I would see this engine idle, 👏👏👏
@Lucius.Hercules
@Lucius.Hercules 13 дней назад
Brilliant work can every upload you push into new territory for greater performance! This is epic 😎
@ArsonalTech
@ArsonalTech 11 дней назад
I’ve never seen a black iron pipe look so nice. Even the new ones usually have a little bit of rust. Fun fact, Dawn dish soap will aggressively rust black iron to a nice bright orange in like 24 hours. (Leak tested a new outdoor gas line and forgot to wipe off the soap)
@CamdenBowen
@CamdenBowen 11 дней назад
That's interesting, I use dawn dish soap as a degreaser for like everything since it's so good and also not horrible for your skin lol, never would have thought
@simonkokoska4384
@simonkokoska4384 13 дней назад
your projects are insane
@spray_cheese
@spray_cheese 11 дней назад
I actually like how this transitioned from a 3D printed engine to an actual engine. I see it as a great way to prototype certain parts. You could take this even further and slowly fabricate each part in metal with plastic prototypes!
@user-gr7py4nu8m
@user-gr7py4nu8m 14 дней назад
i've been waiting this video since months, thank you Bowen
@wyattprout
@wyattprout 13 дней назад
please never stop improving this engine
@herzogsbuick
@herzogsbuick 8 дней назад
you're in the great tropical southlands of canada, while i'm your neighbor to the north in alaska, and i've been able to keep my garage door open for weeks now. maybe the engine had trouble because it didn't have enough oxygen heh watching your progress has been great, thanks for keeping at it, keep 'em comin'
@CharlesVanNoland
@CharlesVanNoland 13 дней назад
Using needlenose pliers to tighten nuts. Takes me back to my crazy 90s kid projects!
@alexlabs4858
@alexlabs4858 13 дней назад
Saw your last video and was super surprised you didn’t have at least one of those vevor mini lathes. I’m sure you’ll make good use of it! I love mine
@Leo.J.G
@Leo.J.G 14 дней назад
WOW im so glad to see this return!!!!
@thekraken4548
@thekraken4548 13 дней назад
Awesome job man, Its fun to watch you engineer and build this this engine. The all success and failures included. build a heavier flywheel or add weights to the inside of the current one and retest. It will make everything more forgiving. then you'll be able to dial in the carb.
@spartan-5795
@spartan-5795 13 дней назад
Certainly an interesting idea to just use a toob from the store as the cylinder "bank". Also, I noticed the bits of music in the video, nice touch! Keep up the good stuff man! : )
@vancemacd6315
@vancemacd6315 13 дней назад
The screw closest to the front of carb is an air Mix screw. The one further back is fuel mixture. Try adjusting while running. Love these videos!
@All_Original
@All_Original 13 дней назад
This is AWSOME!! Great work!!
@chemicalcorrosion
@chemicalcorrosion 13 дней назад
I just ❤ your tenacity!
@2T-projects
@2T-projects 14 дней назад
The engine looks really cool, good work but could you mabey make it a 2t
@onefastgmc
@onefastgmc 13 дней назад
Impressive! This is definitely the kind of stuffni like watching!
@jacketspritecranberry4876
@jacketspritecranberry4876 10 дней назад
Those mixture screws you were adjusting are the idle mixture screws, it seems like the engine needs more fuel all together. Take the screw cap off of the top of the carb and pull the slide out, there should be a little needle coming out of the bottom of the slide. Take out that needle and you should see multiple notches cut out of the needle and a c clip. If you take the clip out and throw it into one of the lower notches it lifts the needle which lets more fuel in. If the clip is too high on the needle, the needle will sit too low in the carb it will be letting barely enough fuel in, and it will cause your idle mixture screws to only be tuned to an extent. Hope this helps👍
@djo_man
@djo_man 7 дней назад
I just had a similar problem at work boring out a 1" hole to within 0.005". I've found that cutting the RPM down can help dramatically.
@alfredkwaak
@alfredkwaak 12 дней назад
nice weld at the cylinder! :D
@FreshlyBounced
@FreshlyBounced 13 дней назад
To mesure precisely a piston you gotta take the mesurements on it's skirt since it"s a little bit wider due to the expansion of the alloy on it's crown, the top heats up lot more than the skirt
@CamdenBowen
@CamdenBowen 13 дней назад
Alot of the handbooks say to measure around 8mm from the base of the skirt to get an accurate reading, but I think they may only apply if the piston has already been used
@alexstromberg7696
@alexstromberg7696 13 дней назад
Pistons are made from the same alloy top to bottom
@Matthews_Media
@Matthews_Media 13 дней назад
Awesome!! Thanks for doing this!!
@awesomecronk7183
@awesomecronk7183 13 дней назад
Well done mate 🎉
@Ruffilicious
@Ruffilicious 10 дней назад
I love your Projekt hope to see more soon
@Mis73rRand0m
@Mis73rRand0m 13 дней назад
You need ignition advance via flyweights and ideally a vacuum diaphragm, in addition to tuning the jets on the carb.
@infinitefray8067
@infinitefray8067 13 дней назад
19:40 based off the faced that that carb is probably for a much larger engine it might be flooding would also explain the smoke coming out of the intake when it shuts off
@Maksenix
@Maksenix 13 дней назад
Finally something interesting on youtube thank you Is really hard to faind this good stuff
@victordinev5229
@victordinev5229 13 дней назад
Hay man, I found your channel yesterday and watched the full series, and i was so excited when the engine was running by itself today. It will be a nice evolution if you try to make fuel i injection with ardoino for example.
@vatonix84
@vatonix84 14 дней назад
was waiting these last few days for it to drop lolz
@PhilTgaming11
@PhilTgaming11 13 дней назад
Finally, revisited and a new video!
@191fox
@191fox 13 дней назад
I think he should make a gear box for it and see how well it goes good job for making it work
@MarcStollmeyer
@MarcStollmeyer 13 дней назад
You should have the valve timing so the exhaust begins to open right before BDC, to reduce load on the engine. Also make an inline 6 with this architecture and run a go cart with it!
@vx-iidu
@vx-iidu 13 дней назад
you got a really good surface finish on the lathe for what it is, cheap lathe with some mystery metal pipe. would've expected way worse
@ThatGuy-bx4yi
@ThatGuy-bx4yi 13 дней назад
Youll probably get more smooth running on the engine when the exhaust tapers in and out with some bends it in. You might not have enough Decompression on the down stroke, still sounds like it's resetting the cycle HARD. That might also explain the explosive down stroke when timing starts to dither. The flywheel wants to keep going and add cycles/torque to compression, the exhaust helps by have gases for the piston to still be expelling, almost acting like an air cushion. If you revisit this, you should show levels of exhaust and differences between em ;)
@Thatdavemarsh
@Thatdavemarsh 10 дней назад
You should add a speeduino to this fantastic mix.
@kaiyofox
@kaiyofox 13 дней назад
it's more impressive to do everything with 3d printed parts like I know a ytber who used to work in all 3d printing and they recently expanded their toolset and it's significantly less fun the challenge of working with 3d printed parts is the way to go but your stuff is still, fairly interesting I get excited when I see a new "3d printed engine" video
@sailing4life467
@sailing4life467 9 дней назад
Hey man a tip for putting on piston rings to make it much easier.. Were the ring split is push one side into the piston slot the lift the other edge of the ring and rotate completely around the piston and it will slot into place
@eadthryth8194
@eadthryth8194 14 дней назад
Haven't watched the video, can already tell it's a banger.
@kakhatsikaradze4772
@kakhatsikaradze4772 13 дней назад
16:10 what a god damn gigachad! Look at that beauty! Edit: very impressive BTW. Small engines like that require a lot of precision. Very well done! Keep going!
@_XRMissie
@_XRMissie 13 дней назад
When you eventually get to turbojet engines, things are going to get nuts lol. This is mighty impressive!
@gazehound
@gazehound 13 дней назад
Please keep building engines this is so cool
@keatyofficial
@keatyofficial 13 дней назад
when you tune a carburetor, make sure you dont have any air leaks, mainly 3d printed parts have microscopic holes, which will make it have a bad air leak, air leaks can cause it to run away, stall, and not even start
@FezzyBus
@FezzyBus 14 дней назад
The engine has a nice idle sound tbh
@gavinhogberg
@gavinhogberg 10 дней назад
Maybe instead of mixing just straight up motor oil into the gas, you could try mixing in some Rotary Engine premix? That's designed to lubricate engine components while being burned, so maybe it'd work
@piganagun9069
@piganagun9069 10 дней назад
Got to love how many stupid mistake sand mishaps you don't edit out, makes me feel better about how much i worse i am at machining
@Scrogan
@Scrogan 13 дней назад
Holy hell, dropping that metal pipe was an instant subscribe button smash. I expect big things from you.
@hayden3928
@hayden3928 13 дней назад
far from 3d printed now, but still a blast to follow and learn about! I'm surprised the bottom end is fine! You must have a serious passion for this now xD
@CamdenBowen
@CamdenBowen 13 дней назад
Thanks for sticking around for so long :)
@haydenc2742
@haydenc2742 13 дней назад
Too much fuel on idle...and probably on the main jets...tighten screws all the way down...back out 2 turns...might need less since it's a big carb and a teeny bore (remember you stepped up size of carb so more fuel per stroke) So awesome to see it hammering along! Keep em coming!!!!
@Alan_Hans__
@Alan_Hans__ 13 дней назад
Absolutely awesome. I think that the facemask and respirator could be used while running the motor.
@andersl.359
@andersl.359 13 дней назад
to fix the issue with heating, if you cant add a radiator, then maybe a water jacket around the cylinder. it could help with keeping temps under control
@merijn1086
@merijn1086 13 дней назад
For a smooth bore, use seemless pipes. That will save lots of work.
@Lilac757
@Lilac757 13 дней назад
The King of Random channel has a couple different videos on how to build pretty good foundries for a decent budget.
@prodigalson2670
@prodigalson2670 13 дней назад
When you eventually buy milling maching, which is inevitable, try getting one with 3phase ac motor, they are good, ones with DC electromotors get fried after a year.
@moneymania5647
@moneymania5647 12 дней назад
IDEA put the enjine on a home made go-cart, love to see more man!
@ThatRandomMan1
@ThatRandomMan1 13 дней назад
You're doing great work brother man! I hope you get big on RU-vid! You definitely should 🤨
@CamdenBowen
@CamdenBowen 13 дней назад
Thanks! Also I'm almost positive I had that exact same bike in your pfp when I was younger lol
@ThatRandomMan1
@ThatRandomMan1 13 дней назад
@@CamdenBowenyou're welcome haha, man i love 450s it's a been a while since I've rode though. 🤔 gonna have to get me another race bike somehow. But that was a 2011 kx450f 🙂 the best bike i owned. I've had many from trading around and rebuilding them. Had a 04 trx450r that was fun too But i'm in a tight spot haha, I'll get out one of these days.
@supers0n1cgam1ng5
@supers0n1cgam1ng5 10 дней назад
HE DID IT. FINALLY. This is dope.
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