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Rapid unscheduled 2GR-FE disassembly 

Frankenstein Motorworks
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27 окт 2024

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Комментарии : 172   
@akinshok
@akinshok 2 дня назад
Embracing mistakes is the first step of learning, an important lesson! Great attitude. It’s heartbreaking and hilarious at the same time! 😂❤
@roachwerks3043
@roachwerks3043 13 дней назад
As an engineering nerd i really appreciate the information and presentation in these videos. your the kind of car guy that every platform needs love the chapter title "new inspection ports" lmao
@future62
@future62 5 месяцев назад
The I Do Cars collaboration I didn't know I needed 😂 Would love to see the last Dyno run (and some of the others). Also wear some gloves man, oil doesn't agree with skin. Thanks as always for the great content
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
I really wish i was recording when it happened. I usually wait until the car is mostly tuned before recording a dyno run so i had not turned on the camera yet. It was sounding amazing making that 330whp. As for gloves, I do try to wear them sometimes but as you notice my hands shake a fair bit and anything that reduces my dexterity further really becomes a problem. I understand it's not ideal though.
@apricity69
@apricity69 5 месяцев назад
Definitely malice in the combustion palace and forbidden glitter.
@mcld4214
@mcld4214 5 месяцев назад
@@FrankensteinMotorworksi hope the shaking is not because of a medical condition. And if it is go get checked out. All love
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
@@mcld4214 I suppose it depends on your definition of "medical condition" but this is something that has always happened to me, it's not getting better and it won't be getting worse. It's just something i have to deal with. no reason for any concern.
@future62
@future62 5 месяцев назад
No worries, you've done more with the hands you were dealt than many! Oddly I've seen some musicians gain dexterity with similar conditions by wearing gloves. Scott's Bass Lessons has a long video on this. Might be worth a look
@contributor7219
@contributor7219 5 месяцев назад
We live and learn, and catastrophic failures like these are something we learn a lot from. I'd say you are spot on about the reason for failure and once that No6 rod bearing started to wear the rod would have hammered those big end bolts to destruction. It's actually a testament to these engines that it lasted long enough to give you useful data.
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
Yeah the motor really did me a solid favor by holding together long enough to get all the data i needed. It was only on the last pull where it was down a bit on power and then the next run it went bang.
@markfox6741
@markfox6741 5 месяцев назад
@@FrankensteinMotorworks What revs were you pulling when it went pop?
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
@@markfox6741 the dyno chart drops to zero right around 6900rpm
@Karsten-cc5ws
@Karsten-cc5ws 4 месяца назад
The sound of dripping metal pebbles when turning the engine over... beautiful! :D
@luisgonzalez3057
@luisgonzalez3057 5 месяцев назад
Nothing some JB Weld can't fix. Looking forward to the next build. Thanks for sharing.
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
I've certainly played that game before, here is one i did on track: www.caranddriver.com/news/a18739056/lemons-goodbad-idea-of-the-week-toyota-fun-with-jb-weld-and-shattered-engine-blocks/
@jamesempson1365
@jamesempson1365 4 месяца назад
You held it together making this video man❤ it must be devastating after so many hours of work
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
Honestly it's not that bad, Toyota made millions of these 2GR-FE engines and the cams survived so this is mostly a loss of time not money.
@rjung_ch
@rjung_ch 5 месяцев назад
That engine took quite a beating. The teardown shows so much. Thanks for sharing this unscheduled disassembly 👍💪✌
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
Hopefully i don't have too many videos like this to show but i do try to show the failures with the successes to be a bit more realistic with how this stuff happens.
@rjung_ch
@rjung_ch 5 месяцев назад
@@FrankensteinMotorworks Naturally that's what I wish as well. But pushing them does take something to hold up. I think it must be the clogging of the oil paths thus the destruction. Good luck figuring it out for us. Thanks again.
@iceyinferno
@iceyinferno 5 месяцев назад
Thanks for putting together a good video on the diagnostics after the failure. Unfortunately, this can be part of the process and it's understandably frustrating. Keep up the good work!
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
Thanks for watching it. I needed to take it apart to learn what happened anyways so i may as well shoot a video and show everyone that not everything is perfect all the time.
@jorgefive0
@jorgefive0 5 месяцев назад
Liking every single one to hopefully influence the algorithm
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
I appreciate it.
@jasonyoung6420
@jasonyoung6420 21 день назад
That motor sounded like a rain stick when you flipped it over 😛 Good stuff, I'll be following your 2GR builds. I don't have an MR2, but I am about to purchase a Sunbeam Alpine; a 2GR that spins to 9,000 RPM sounds like a great swap candidate (I have a RWD IS350 F-sport as a daily).
@dejitalone
@dejitalone 5 месяцев назад
The good, the bad and the ugly. Thanks for sharing all seasons of your performance journey Marc! (RIP 2GR lol)
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
Thankfully Toyota made plenty of these engines and there's no shortage of them. So we learn, maybe make some entertainment and then move on. Thanks for watching the video.
@Syncopia
@Syncopia 4 месяца назад
Malice in the combustion palace!
@zackreichert464
@zackreichert464 5 месяцев назад
After sending several 5S and 3S motors to the great beyond I'm glad to hear that's why you went with a V6 swap many moons ago. I was originally going to swap a 1MZ/3MZ into my Celica, but then I heard about a guy across the state line swapping 2GRs into MR2s. The rest is history. I'll at least have the GR and the Solara box mated and in the car this summer. Thank you for all that you do Marc.
@torew01
@torew01 5 месяцев назад
Oh, that painful smile.. I once did vibration measurements during trials on a new model water injecton pump. 10 MW, 360 bar, 8000 rpm centrifugal pump. It started sounding strange, so we dropped the speed to 4000 rpm. From there it just stopped in 0.5 seconds. Took the workshop 2 weeks to cut it open with angle grinders to find out what had happened...
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
It's impressive how these systems can go from perfectly fine to just a giant pile of scrap. I can't even imagine what a 10MW pump looks like, that has to be huge.
@torew01
@torew01 5 месяцев назад
@@FrankensteinMotorworks Yeah, in this case it was a mistake in the design, that made the axial bearing clearance increase with temperature and pressure, causing the impellers to rub the housing. It worked until it didn't. Fun times... Actually, it isn't that big, but had around 15 cm thick walls. The high pressure takes a lot of power out of a relatively small pump.
@jeffreymoore4132
@jeffreymoore4132 5 месяцев назад
The shower of pieces that fell from the crankcase is an amazing amount of desstruction. Thank you for bringing us along the diagnosis journey. I find these just as informative as the R&D more horsepower ones.
@mikeshock7265
@mikeshock7265 4 месяца назад
Id love to be at your level of knowledge one day. Great video.
@CM-tc6pp
@CM-tc6pp 4 месяца назад
It's funny that I came across your video because I just had a nightmare in which I started my car without oil. I was in the middle of an oil change, became distracted, and then started my car. I remember turning the key and realizing I hadn't put oil back in it and just couldn't stop myself in time. The sound the engine made was excruciating and I was devastated. I was so relieved when I woke up...Sorry this happened but you seem to be taking it in stride.
@hendoglenn6868
@hendoglenn6868 4 месяца назад
"Interesting data on the top of that piston", Lots of data, everywhere :). Great video with a good sense of humor about a not so good situation. I hope all goes well on your next build :)
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
Glad you enjoyed it and yeah i think the next build will go a bit better than this one :)
@gabzor4716
@gabzor4716 4 месяца назад
Rapid disassembly indeed, love to see how excited you are about all the destruction lmao
@navseal345
@navseal345 4 месяца назад
That is an amazing aftermath of rapid unscheduled disassembly.
@angusmacsac
@angusmacsac 5 месяцев назад
I’m sorry but the sounds in this vid are just too funny!
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
I agree, i was laughing my ass off while editing seeing all the parts fall out whenever i shifted it.
@rjung_ch
@rjung_ch 5 месяцев назад
that did make horrible sounds...I laughed as well.
@neilfreytag9166
@neilfreytag9166 5 месяцев назад
14:38 "rear main seals off" 🤣
@desertfresh3740
@desertfresh3740 4 месяца назад
I love your attitude about this, and not only recognizing but owning that it's your own fault. That's big of you. 👍
@stansbruv3169
@stansbruv3169 4 месяца назад
Your transparency along with your experience and knowledge are appreciated!!
@papapetad
@papapetad 4 месяца назад
Sad dyno day but a solid number of pulls and mileage out of it considering. That was one for science and it got you going down this path. All is well :)
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
Yes, at the end of the day this is just the cost of doing business. It's bound to happen eventually.
@Alvin1620
@Alvin1620 4 месяца назад
Great video! My son and I have learned so much from your videos.
@noahmckinney2455
@noahmckinney2455 4 месяца назад
I run a 3sfe Cummins turbo motor in my mk2 Supra. It’s over heated a few times and rod bearing noise once. I’ve been thru it a few times and it’s amazing I haven’t had this rapid disassembly running 17psi and over 22psi a handful of times. Especially since I made my own intake causing weld beads to run in my cylinder. Cylinder 3 looks like the surface of the moon and it’s been daily driven and drifted for around 7 months now. Just popped a head from 3x reused head bolts. It’s getting arp studs next. I don’t like 3sg engines either but these f heads are stout
@Aquarius2937
@Aquarius2937 4 месяца назад
yeah, your engine should not sound like a pachinko machine when it turns over :P That being said, don't stop your great work, sir.
@13harward
@13harward 5 месяцев назад
Commiserations on the blow up, that really was quite extensive. But... as you've already said, a chance to learn. Loving the open and honest nature of the video too, it must've been a sickening noise when the engine let go! Onwards and upwards! 🙌🤝🤝🤝
@brian6029
@brian6029 4 месяца назад
That sucks that happened. Glad you showed us so we can learn from it as well.
@gahirst
@gahirst 4 месяца назад
I know the pain. Two years ago I had my engine disassemble, probably because we tried 12psi of boost on a stock engine. I noticed "white fluff" in the filter, when I was services it before taking it to the track. Pretty sure that was a spun bearing. Piston in a million pieces, connecting rod in maybe 7 pieces, no inspection holes. Recent one may have been the same thing, but maybe due to aerated oil or slightly low level, going through hard right hander at high revs. Still haven't pulled that one apart yet.
@timwise6876
@timwise6876 4 месяца назад
Ouch, too bad Marc, interesting tear down thanks. The sump turned into a scrap metal bin.... All the best from your Mates in Aus 😆
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
yeah it really did turn into fine dust. but it's just a cost of doing R&D sometimes.
@romariojarrett6889
@romariojarrett6889 5 месяцев назад
Try out the 2gr fks u got laying around. The is350 community would of loved that 😭
@jonmac155
@jonmac155 5 месяцев назад
Laughing my ass off when you turned the motor upside down. The noise was gold. Otherwise sorry about your motor.
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
yeah i was laughing pretty hard when i was editing the video. it was gold and i needed to leave that stuff in the edit :)
@DV7Dave
@DV7Dave 5 месяцев назад
Wow! I've never seen so many metal shavings in one block. Are you going to film the new 2GR build? Maybe the new engine will make even more power!
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
I think there was at least another 5whp left in it the way it was and it's possible there was some internal drag too so who knows. I will be rebuilding it but with higher compression pistons next time so it makes over 350whp but who knows, maybe 360whp?
@mrkazman
@mrkazman 4 месяца назад
blessed content from the Toyota angel.
@nickzaccheo9294
@nickzaccheo9294 5 месяцев назад
Thank you for all you do! You keep my dream alive for my SW20.
@aw11man26
@aw11man26 4 месяца назад
2 things I love about this video. 1:the sound of gravel in a bucket everytime the engine is turned over. 2:A grown man laughing about the extent of his own self induced catastrophic failure...lol
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
Yeah there's really no point in getting mad at it. what's done is done and thankfully at the end of the day the cams survived so the only thing lost is an engine that Toyota has made millions of copies of so it won't be hard or particularly expensive to replace.
@markfox6741
@markfox6741 5 месяцев назад
I shouldn't have, but I laughed then first time you turned the motor upside-down... however, I did wince when you turned it back the right-way-up! I think I recognise the pissed-off-with-self 'shouldawouldacoulda' feeling. Right there with you brother. When die-castings get 'impacted' they really get hammered, don't they? Surprised you didn't have double-glazing salesmen knocking on the garage door to fill up those new inspection ports. Bank 2 reveal was pretty special... Rear main seal removal: *LOL*! Good luck finding a new core and getting Natasha back in the V6 way.
@tedmich
@tedmich 4 месяца назад
😳total carnage! New engine time ! 😂We appreciate the omelets, a few broken eggs are expected!
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
Yeah it was bound to happen eventually with all the experimenting around. I'm just glad it was a stupid mistake from me not a flaw with the motor that i needed to start finding a fix for.
@jamesempson1365
@jamesempson1365 4 месяца назад
I always love the gr series of kids I really want to import a 2012 crown athlete with a 2gr-fse
@DavyDave123
@DavyDave123 4 месяца назад
It's like I went to the Frankenstein Motorworks channel and the I Do Cars channel came up. You guys could have done a nice crossover/cross promotion video together disassembling that engine.
@Neudezign
@Neudezign 5 месяцев назад
Wow! I'm definitely NOT an engine expert, but I would guess this constitutes as: Catastrophic! Dude, when you first flipped the engine over it sounded like a bag of Skittles being tossed about. Ouch, sorry to see this happen, but definitely appreciate you doing a tear down. Very informative and appreciate you giving us your insight and explaining what went wrong and what parts to look at. I guess your loss, is our education... I'm sure that doesn't necessarily console you very much, sorry. 🙁 Hey, I guess if you ain't blow'n something up once and while then you probably ain't having any fun 😅👍🛠 Keep on wrenching!
@Thelegoman901
@Thelegoman901 5 месяцев назад
A little ventilated compression never hurt anybody
@daniel9111
@daniel9111 4 месяца назад
Doing it for science!
@dannoyes4493
@dannoyes4493 5 месяцев назад
Bless your heart.
@supers0nic77
@supers0nic77 4 месяца назад
I really want to get one of these engines for mine!
@grad0n
@grad0n 5 месяцев назад
Proper Carnage!
@dfsfdsfsdfsdfsadsdfsfdsdsf3587
@dfsfdsfsdfsdfsadsdfsfdsdsf3587 4 месяца назад
Ive torn one of these failures before. All you can do is save and label the hardware because everything is trash except the valve and timing covers. Oh yeah i saved the chain, balancer, crank position ring and oil pickup too.
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
In this case the valve covers are actually quite known for accumulating grit when powdercoated so i'll be tossing those too and the timing cover is the oil pump so that's also getting pitched. But the good news is the cams are still straight so the expensive part is still good.
@dfsfdsfsdfsdfsadsdfsfdsdsf3587
@dfsfdsfsdfsdfsadsdfsfdsdsf3587 4 месяца назад
@@FrankensteinMotorworks Mine was a 2zz I found for $35. You can guess what happened to it the cams were wiped.
@joshuavincent7884
@joshuavincent7884 5 месяцев назад
piece of paper taped to the steering wheel with big bold letters "HAS NO OIL"
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
Yeah the issue is that it got pushed out of the shop to get the race car prepped for a race and then two weeks later i got back to it. a note would have been helpful for sure.
@Pippy1
@Pippy1 4 месяца назад
I always like to pull the key and put it on my toolbox whenever i have to leave a car without oil. Means i have to think about getting that key to start it
@T.R.A.N.C.E
@T.R.A.N.C.E 4 месяца назад
my condolences.
@justintowers8230
@justintowers8230 4 месяца назад
sorry to hear bout the oil starvation. i did this with my 3sge beams redtop. drained the oil but didnt replace the oil filter. had it idling for 5 min before realizing it had no oil. oil pressure light never came on. hoping not to have shavings in my oil filter and oil pan.
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
Hopefully you got away with it. For what it's worth i think my situation was much worse because i used brake clean to clean the flywheel flange and that washed the oil out from the #4 main.
@el_bigoton1377
@el_bigoton1377 3 месяца назад
I really love all your content! Very informative and detailed oriented videos. I have a question for you would you ever consider looking into the A25A-FKS ? I’m curious because the thing has some pretty high compression for a low hp 4cyl, would be interesting to see one make 300 NA, but thats just me dreaming haha, i would like your input though if it would even be worth to do? I did see your 2GR-FKS teardown and was pleasantly surprised with what you found and was wondering if the engine could be similar to the A25A-FKS in any way like the 2AR-FE to the 2GR-FE.
@FrankensteinMotorworks
@FrankensteinMotorworks 3 месяца назад
I actually have an A25A-FKS here because i wanted to explore it and i do think it's a great motor but it just does not have anywhere near the same potential as the 2AR-FE. the valves are tiny, the stroke is enormous, the ports just aren't big enough and the runners in the head on the exhaust side are going to require a lot of work to fix some of the compromises they did in there to fit the EGR system.
@yung.letuce
@yung.letuce 4 месяца назад
Off Topic but I have a 2006 IS350 with the 2GR-FSE and A. Was wondering if you’ve considered using that platform and B. Have you considered cams? ( I just found your channel not sure if you have) I’m chasing 350 haha
@andycraig6905
@andycraig6905 5 месяцев назад
Blew up my 2004 camrys 2azfe by letting it burn all the oil up and spin a bearing. Caught it too late, oil wasn't touching the dip stick. Probably roasted a piston ring because it took no time to eat all the oil
@jonasahgren
@jonasahgren 4 месяца назад
I have just honed my block 2GR-FE and the new forged piston from Wiseco now have a wall clearance of 0.0043" instead of from Wiseco recommended 0.003". Should i get oversized pistons and start over? The engine is supercharged and will make around 5-600hp. Right now its at 480hp on stock internals witch is a push for track-use. I also have the Kelford 263 A cams, springs and forged rods. But that doesnt matter.
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
Are you sure it actually recommended 0.003"? that's a bit tight even without a supercharger. I would expect a 0.004-0.005" clearance requirement but it really comes down to the piston material and how much it expands so you should go with what the piston manufacturer recommends.
@fallenfather4469
@fallenfather4469 5 месяцев назад
Hahaaa learned my lesson with the no oil lol!
@PRZJ91
@PRZJ91 4 месяца назад
The other head can be saved! Don’t scrap it! Might take a little money to get the bowl touched by a cnc machine but it’s fixable!
@p0lytube
@p0lytube 4 месяца назад
in terms of number of metal chunks, one of the most catastrophic failures i can think of
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
the motor let go at 6900rpm while making about 300whp so it had a hell of a lot of energy in the system to really make everything rattle around in there and turn to dust.
@jtto6364
@jtto6364 5 месяцев назад
Go big or go home. I'm sure JB weld can fix it, hehe Cheers:):):)
@guntrain212
@guntrain212 4 месяца назад
Out of curiosity, given how Mike Reed's Apex Mr2 blew up on the road course (and he consequently lowered his 8k redline), could this be related to an oil starvation issue at higher rpm?
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
I don't think that's the case here given where the damage was matched up exactly with the previous dry start damage. But with that said, above 8000rpm there's certainly a lot of unknowns yet to be discovered.
@ShootingWithPhil2023
@ShootingWithPhil2023 5 месяцев назад
Nice title for the video...LOL!
@turbyturbo1
@turbyturbo1 4 месяца назад
2gr ftw
@ChrisWilson-rf8cs
@ChrisWilson-rf8cs 5 месяцев назад
Talk to Papadakis about the valvetrain mod they did...
@rozap_8356
@rozap_8356 4 месяца назад
I started an engine in my lemons car with the remote oil filter plumbed backwards. Similar results. Feels dumb but happens to everyone.
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
Yeah i did that on a ford 302 back in the day. That's when i learned that oil filters are directional. I completely destroyed the top end of that motor in about 5 miles
@modeverything1
@modeverything1 4 месяца назад
Sacrifice for science!
@dand6119
@dand6119 Месяц назад
Is it possible to get a low LSA camshaft and throw it into a 3.5Tacoma 2gr-fe
@joemamaisobama5788
@joemamaisobama5788 4 месяца назад
The 2gr v6 is the first platform I’ll be building in my life albeit it’s the 2gr fks. I saw your 404 whp big cam high comp piston 2gr fe on instagram and thought you’d be the right person to ask, but how would you go on about making 310-330 whp and 300 wtq?
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
The question as stated is completely achievable but i think what you're actually asking is to make a big displacement V8 power curve with a 3.5L engine. You want that torque to happen at low RPM but when you lose displacement you need to make up for it with RPM or boost. I get this kind of question from truck people all the time so i'm going to assume you're in a truck so on top of that you have a much higher drivetrain loss than the application i'm doing here. This means you'd need about 170-180% cylinder fill to hit those numbers, you're talking about essentially building what would be a 500whp+ NA build but then just not letting it rev past about 5500rpm so you still have all the costs associated with a 500whp+ NA build. Hitting your actual goal will be best done with a supercharger or an engine swap with more displacement.
@joemamaisobama5788
@joemamaisobama5788 4 месяца назад
@@FrankensteinMotorworks my bad I should’ve specified I’m in the 8th gen fwd v6 Camry. 500 whp+ na build seems very difficult to pull off on any v6 so mabye a supercharger would be the way for that low end torque. The only thing is tho the only supercharger kit for the 8th gen cams are still under R/D and also I’m not sure if the transmission could handle all that torque even with a full rebuild so I was kinda hoping there were some bolt on mods that increase low end tq
@SimanSlivar
@SimanSlivar 5 месяцев назад
By any chance have you checked the oil pressure data during your pulls? I found that mine had issues under load and shifting. When the pressure place was rengaged the oil pressure would drop off a cliff. I concluded the crank was bending when the pressure plate reengaged increased the shift dwell time to help it out.
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
Unfortunately I do not have any oil pressure logging on these pulls. but looking back on the logs i can see the power drop a bit on the previous pull at about 7000 when the bearing must have started really getting some damage and then the last pull came apart at 6900rpm.
@SimanSlivar
@SimanSlivar 4 месяца назад
Hmm 🤔 I wonder if these 2gr cranks have issues. Wouldn't be a first with my yota engines the crank flex...
@michaelbleazard3179
@michaelbleazard3179 7 дней назад
Do you have a site or something? I do have a 2gr-fe engine in my es350, I am hoping to get little more power from it if I can
@FrankensteinMotorworks
@FrankensteinMotorworks 6 дней назад
frankensteinmotorworks.com but the reality is you need an exhaust system before anything else an i don't have any offerings for non MR2 exhaust parts.
@melo.lucas320
@melo.lucas320 5 месяцев назад
That engine bit the dust......
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
Yeah it really turned to dust. It blew up on the dyno at 6900rpm so there was a lot of energy in that disassembly.
@melo.lucas320
@melo.lucas320 5 месяцев назад
@@FrankensteinMotorworks whoops....
@sebastianromero420
@sebastianromero420 4 месяца назад
An OG Honda engine is impervious to oil starvation
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
absolutely, taking the oil out is the key to making that 1000whp that everyone says they can make. no further modification necessary.
@sebastianromero420
@sebastianromero420 4 месяца назад
@@FrankensteinMotorworks so true 😂
@bspiritracing
@bspiritracing 5 месяцев назад
Holy smokes that thing is eaten up!
@Thri11seeker
@Thri11seeker 4 месяца назад
Also weird question but is the 9k rpm build manageable still have yet to see anyone prove it working
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
I'm looking forward to figuring it out, it's going to take a minute since there are competing priorities but it's work in progress.
@Thri11seeker
@Thri11seeker 4 месяца назад
@@FrankensteinMotorworks I was about worried to hear this was the outcome of it because I may be doing a build like this sooner then I planned
@rimka11
@rimka11 5 месяцев назад
But why three cylinders? What caused the other two?
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
just all the debris in the crank case catches other things in there. the engine let go at 6900rpm so things were moving in there and it all just quickly became a mess.
@Gangstazombies_1
@Gangstazombies_1 4 месяца назад
Where can I get headers for 07 Camry 2gr
@bryanhutson6741
@bryanhutson6741 4 месяца назад
Now that it's dead, can you swap this out for a FKS?
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
I have inspected the 2GR-FKS and while it is a good motor it has a lot less potential than the 2GR-FE. That integrated header situation is a significant impediment to big NA power. Direct injection is also really nice for a street car but just adds a much more expensive ECU to control it all when you push this hard on it.
@brudevold62
@brudevold62 4 месяца назад
Is there any benefits from swapping in 2ur valve train components?
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
The lighter intake valves in theory help you rev higher but realistically that isn't needed until you get to much higher RPM builds. I will be using these for my 9000rpm build.
@romariojarrett6889
@romariojarrett6889 5 месяцев назад
The painful laugh 🤣
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
Getting angry certainly won't help :)
@TimMutton317
@TimMutton317 5 месяцев назад
How much HP until it blew?
@matthewgriffiths527
@matthewgriffiths527 5 месяцев назад
It looks as if you have essential tremors in your hands.
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
Yeah, it's better some days than others. It's annoying but i don't let it slow me down.
@grad0n
@grad0n 5 месяцев назад
CBD
@driftke70
@driftke70 5 месяцев назад
@@FrankensteinMotorworks i have the same thing dont even notice it anymore. Doesnt impact me in any way. Definitely some good days and bad.
@andycraig6905
@andycraig6905 5 месяцев назад
​@@grad0nbest option for workers, you get the medical benefits but you can keep a clear head and get your work done safely
@burntbisquit7633
@burntbisquit7633 4 месяца назад
Why are you not fan of the 3sgte?
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
It was a fantastic motor for it's time but this was a motor designed in the late 70's. The head on the 3S-GTE is a slightly newer design but less than a decade newer. Motor technology and material strength has moved so far forward since then and my whole thing has always been to take advantage of modern engine technology. Consider that the 2AR that i play with makes 25% more power to the wheels than the 3S-GTE in the MR2 and that's before you open it up and do anything to it and that's also without any boost. Sure it has 25% more displacement but it also does not have 10psi of boost being shoved into it.
@burntbisquit7633
@burntbisquit7633 4 месяца назад
@@FrankensteinMotorworks that makes sense. Plus, parts are probably easier to source with the 2AR compared to the 3sgte nowadays.
@kingmarz3635
@kingmarz3635 4 месяца назад
Should have gone with the Honda J series engine, far more compact and has none of the many 2GR issues
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
Which "many" 2GR issues are you talking about? The 2GR really does not have any critical issues in it. This motor blew up because i accidentally ran it without oil, no motor would survive that.
@kingmarz3635
@kingmarz3635 4 месяца назад
Issues like leaking water pumps, leaking timing cover, cam gear death rattle all of which require engine out in camry layout which is 20-24 hours labor Worst engine layout in the world
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
I will give you that the order that is required for disassembly by the way the timing cover and upper oil pan connect is less than convenient everything else listed here is a 2008 or earlier problem that Toyota fixed way early in the production run and even if you get one of those for your swap it's trivial and cheap to fix. "leaky water pumps" was one batch of water pumps in 2007 that they recalled and fixed. The impelers weren't pushed in far enough on there which caused interference. Leaking timing cover was also an early engine problem, trivial to solve when swapping an engine in with a couple dollars worth of RTV but very few of them actually leaked anyways. The cam phaser rattle issue was a 2008 problem, they did not recall this but they issued a TSB to repair all the ones that were rattling. If you don't count the Lotus application where it's still in production Toyota had the 2GR-FE in production from the 2005 model year to the 2019 model year, 14 years of production and most models did not start until the 2007 model year so you're talking about a very small percentage of these motors, the newest of which is 16 years old, it's just not likely to be one you run into and even if you do it's cheap to address before the swap.
@kingmarz3635
@kingmarz3635 4 месяца назад
Ahh You’ve talked up the shit engine longer than your 2GR has lasted I as a mechanic refused to do work on a fwd 2gr Never again!
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
@@kingmarz3635It sounds like your issues may have more to do with the chassis they wrap around these things making working on the engine difficult. This may or may not be valid i don't really have experience with it in the stock chassis. Either way, enjoy the Honda engines that's the beauty of there being multiple manufacturers out there. I'll be here enjoying these Toyota engines.
@jrmotorsports5532
@jrmotorsports5532 5 месяцев назад
KA-BLAMO!
@kingdavid2018
@kingdavid2018 4 месяца назад
Honerable fate
@1magnit
@1magnit 5 месяцев назад
Looks like you didn't torque up no 6 properly.
@FrankensteinMotorworks
@FrankensteinMotorworks 5 месяцев назад
This is entirely possible but it's generally unlikely for two things to fail at the same time and the #6 not being torqued properly will not cause any damage to the #4 main so the damage on #4 would indicate that it was likely torqued properly. I never did find the 2nd conrod bolt so i could not see the evidence there. Also, i've made the mistake of not torquing the conrod bolts properly before and oh my god that makes a noise you can't miss and there was none of that here. None of this is concrete proof but i really believe that everything was torqued properly.
@1magnit
@1magnit 4 месяца назад
@@FrankensteinMotorworks When no 6 undoes it's self it hits no 4.
@Milkmans_Son
@Milkmans_Son 4 месяца назад
Is it weird it didn't knock? Seems weird it didn't knock. Anyway, I probably would have cooked up some stupid not a lie but not the truth excuse like "oh, man, there just wasn't enough zinc in the break in oil I went with... "
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
Yeah it really is odd the only sign it gave was a bit of a loss of power on the previous dyno pull but i was in process of getting the timing dialed in so it just seemed overly sensitive to the 2degrees less timing above 7000rpm or so but then on the next pull it went bang.
@grippgoat
@grippgoat 4 месяца назад
That's not an engine. That's a V6 Piñata! 😂🪅
@ReignitedAuto
@ReignitedAuto 5 месяцев назад
My favorite Elon musk expression 😂
@jasimalnaimi9669
@jasimalnaimi9669 4 месяца назад
😢
@OhOmah
@OhOmah 4 месяца назад
Ban Omar
@GuidoRugo
@GuidoRugo 2 месяца назад
K-swap incoming?
@ryshask
@ryshask 4 месяца назад
2:40 D:
@km6832
@km6832 4 месяца назад
His shaking worries me...
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
It annoys me but i promise I'm am on top of taking care of my medical. Please don't worry about it.
@stirch9
@stirch9 5 месяцев назад
First
@PracticalRecycling101
@PracticalRecycling101 4 месяца назад
Sorry man. Out of interest. How much would that motor cost to replace? And how much time to buy it. Prep it and install it?
@FrankensteinMotorworks
@FrankensteinMotorworks 4 месяца назад
Depending on what kind of deal you get on it the motor itself not the parts bolted it on the outside that survive just fine is $250-$1500 or so. installing cams in it like i did for this build is about 2hours, installation is about 4-5 hours. It's not bad at all.
@PracticalRecycling101
@PracticalRecycling101 4 месяца назад
@@FrankensteinMotorworks thanks for the info. Doesn't sound too heavy.
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